ASN Wikibase Occurrence # 360851
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 9 February 1994 |
Time: | 22:10 LT |
Type: | Boeing 737-130 |
Owner/operator: | Continental Airlines |
Registration: | N408PE |
MSN: | 19025/32 |
Total airframe hrs: | 59618 hours |
Engine model: | P&W JT8-9A |
Fatalities: | Fatalities: 0 / Occupants: 100 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Chicago, IL -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Newark, NJ (KEWR) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:BEFORE DEPARTURE THE AIRLINE HAD MAINTENANCE PERFORMED ON THE AIRPLANE. UPON COMPLETION OF MAINTENANCE MECHANICS REMOVED THE WHEEL CHOCKS AND TOWED THE AIRPLANE TO THE DEPARTURE GATE. A PRE-FLIGHT INSPECTION OF THE AIRPLANE WAS COMPLETED BY THE FIRST OFFICER. SHORTLY BEFORE PUSHBACK, THE LEAD SAFETY AGENT INSPECTED THE AIRPLANE. WHILE MAKING ITS LANDING APPROACH THE FIRST OFFICER COMMANDED LANDING GEAR DOWN. TWO GREEN LANDING GEAR SAFE LIGHTS WERE OBSERVED. ONE LANDING GEAR UNSAFE LIGHT ILLUMINATED. THE CREW DECIDED THE LEFT LANDING GEAR WOULD NOT EXTEND AFTER MANY ATTEMPTS. THE CAPTAIN LANDED THE AIRPLANE WITH THE LEFT MAIN LANDING GEAR PARTIALLY EXTENDED. THE ON-SCENE INVESTIGATION REVEALED WHEEL CHOCKS WEDGED BETWEEN THE WHEEL WELL LIP AND INSIDE LEFT MAIN GEAR TIRE. THE COMPANY HAD NOT ESTABLISHED PROCEDURES CONCERNING PLACEMENT OF WHEEL CHOCKS BY ITS MAINTENANCE, FLIGHT, AND GROUND SERVICE PERSONNEL.
Probable Cause: AN INADEQUATE PROCEDURE FOR HANDLING OF WHEEL CHOCKS BY COMPANY MAINTENANCE AND OPERATIONS PERSONNEL. FACTORS ASSOCIATED WITH THIS ACCIDENT WERE AN INADEQUATE INSPECTION OF THE AIRPLANE BY COMPANY MAINTENANCE PERSONNEL, AND AN INADEQUATE PRE-FLIGHT INSPECTION BY THE CO-PILOT.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI94IA081 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB CHI94IA081
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 11:50 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation