ASN Wikibase Occurrence # 361280
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 19 September 1993 |
Time: | 11:00 LT |
Type: | Mooney M20C |
Owner/operator: | Ideal Helicopter Service, Inc. |
Registration: | N6752N |
MSN: | 680066 |
Year of manufacture: | 1968 |
Total airframe hrs: | 4402 hours |
Engine model: | LYCOMING O-360-A1D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Crivitz, WI -
United States of America
|
Phase: | Initial climb |
Nature: | Executive |
Departure airport: | |
Destination airport: | Sullivan, WI (31WI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane had a total loss of engine power shortly after takeoff. The pilot attempted to restart without success, and made a hard landing in a field. The right fuel tank strainer was found to be blocked by foreign material.
Probable Cause: fuel starvation caused by foreign matter in the fuel tank strainer.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI93LA367 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB CHI93LA367
Location
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 16:43 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation