ASN Wikibase Occurrence # 361545
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Date: | Wednesday 4 August 1993 |
Time: | 10:30 LT |
Type: | Kit Fox IV |
Owner/operator: | Private |
Registration: | N127RF |
MSN: | 1467 |
Total airframe hrs: | 63 hours |
Engine model: | ROTAX 912 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Green Bay, WI -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AMATUER BUILT AIRPLANE SUSTAINED A TOTAL LOSS OF ENGINE POWER WHILE IN CRUISE FLIGHT. DURING THE FORCED LANDING THE AIRPLANE SUSTAINED SUBSTANTIAL DAMAGE. A POST ACCIDENT EXAMINATION REVEALED THAT A FUEL SYSTEM SCREEN WAS BLOCKED WITH A SUBSTANCE THE PILOT-IN-COMMAND STATED WAS A SEALING COMPOUND HE HAD USED IN THE FUEL TANK. THE PILOT STATED HE DID NOT REMOVE THE FUEL SCREEN WHILE PERFORMING MAINTENANCE ON THE FUEL SYSTEM.
Probable Cause: the improper modification of the fuel system by the pilot-in-command. A factor was bockage of the fuel system screen.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI93DEP03 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB CHI93DEP03
Location
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 19:35 |
ASN Update Bot |
Added |
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