ASN Wikibase Occurrence # 361678
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Date: | Wednesday 14 July 1993 |
Time: | 16:35 LT |
Type: | Brown GLASSAIR SH-2 |
Owner/operator: | Private |
Registration: | N412NV |
MSN: | 332 |
Total airframe hrs: | 272 hours |
Engine model: | LYCOMING O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Timmonsville, SC -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Monroe, NC (KEQY) |
Destination airport: | (58J) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED THAT THE ENGINE STARTED RUNNING ROUGHLY WHILE ON APPROACH TO RUNWAY 32. BECAUSE HE WAS TOO HIGH FOR A SAFE TOUCHDOWN AND ROLLOUT, THE PILOT ATTEMPTIED A FORCED LANDING TO A FIELD ADJACENT TO THE AIRPORT. DURING THE FORCED LANDING, THE AIRPLANE WAS DAMAGED. THE EXAMINATION OF THE AIRPLANE AND ACCIDENT SITE DISCLOSED THAT THERE WAS NO FUEL IN THE FUEL TANKS NOR WAS THERE FUEL SPILLED IN THE IMMEDIATE VICINITY OF THE MAIN WRECKAGE. THE AIRPLANE WAS LAST REFUELED THREE WEEKS PRIOR TO THIS FLIGHT, AND HAD FLOWN ABOUT TWO HOURS PRIOR TO THIS FLIGHT. THE PILOT ESTIMATED A TOTAL FUEL ENDURANCE OF FOUR AND ONE HALF HOURS; THE FUEL GUAGE INDICATED ABOUT 22 GALLONS OF FUEL ON BOARD AT HIS LAST DEPARTURE. THE PILOT ALSO REPORTED THAT, N412NV HAD A HISTORY OF VENTING LARGE QUANTITIES OF FUEL WHILE PARKED ON THE RAMP. ACCORDING TO THE PILOT, STODDARD-HAMILTON (GLASSAIRE), ISSUED A SERVICE BULLETIN TO CORRECT THE FUEL VENTING PROBLEM; THE SERVICE BULLETIN HAD NOT BEEN ACCOMPLISHED ON N421NV.
Probable Cause: THE PILOT'S INADEQUATE FUEL PLANNING WHICH RESULTED IN THE EXHAUSTION OF THE FUEL SUPPLY AND THE LOSS OF ENGINE POWER. A FACTOR WAS THE PILOT'S FAILURE TO COMPLY WITH A MANUFACTURER'S SERVICE BULLETIN.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL93LA128 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB ATL93LA128
Location
Revision history:
Date/time | Contributor | Updates |
17-Mar-2024 06:37 |
ASN Update Bot |
Added |
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