ASN Wikibase Occurrence # 361765
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Date: | Wednesday 30 June 1993 |
Time: | 19:45 LT |
Type: | Mooney M20J |
Owner/operator: | Private |
Registration: | N3740H |
MSN: | 24-0917 |
Total airframe hrs: | 900 hours |
Engine model: | LYCOMING IO-360-A3BC |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Spring, TX -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | (KDWH) |
Destination airport: | (KDWH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE ON CLIMBOUT FROM THE AIRPORT, THE PILOT REPORTED TO THE TOWER THAT HE HAD AN ENGINE PROBLEM AND HE WAS IMMEDIATELY CLEARED TO LAND. THE PILOT OVERSHOT THE RUNWAY AND AS HE APPROACHED THE DEPARTURE END, HE ESTABLISHED A VERY HIGH CLIMB ANGLE IN AN ATTEMPT TO CLEAR POWERLINES AND TREES. CONTROL WAS LOST AND THE AIRPLANE IMPACTED IN HEAVILY WOODED AREA IN A NOSE DOWN ATTITUDE. AN ENGINE TEARDOWN REVEALED CORROSION AND CORROSION PITTING THROUGHOUT THE INTERIOR OF THE ENGINE.
Probable Cause: THE PILOT'S IMPROPERLY PLANNED APPROACH AND THE RESULTANT OVERSHOOT OF THE INTENDED LANDING AREA. FACTORS WERE THE PARTIAL POWER LOSS DUE TO INTERNAL CORROSION, AND THE INADVERTENT STALL.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW93LA201 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB FTW93LA201
Location
Revision history:
Date/time | Contributor | Updates |
17-Mar-2024 07:28 |
ASN Update Bot |
Added |
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