ASN Wikibase Occurrence # 36186
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Date: | Saturday 28 December 1996 |
Time: | 11:09 LT |
Type: | Mooney M20C |
Owner/operator: | Wayne A. Fleming |
Registration: | N7773M |
MSN: | 20-0019 |
Total airframe hrs: | 2748 hours |
Engine model: | Lycoming IO-360-A1D |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Roxboro, NC -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | (KTDF) |
Destination airport: | Mt Airy, NC (KMWK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Shortly after takeoff in instrument meteorological conditions (IMC), the pilot made an initial radio call to approach control (ATC), then about 35 seconds later, he annouced, 'I've just lost my vacuum.' Air traffic controllers attempted to assist the pilot, but were unable to communicate with him further. Radar data showed the airplane made a left turn and climbed to 1,400 ft. After about 270 degrees of turn, the airplane's flight path became erratic. The airplane was last depicted at 1,300 ft and 2 miles south of the airport. About 4 minutes after takeoff, it collided with wooded terrain in uncontrolled flight. During the investigation, no specific reason was found for the reported loss of vacuum; however, during impact, extensive damage of the airplane occurred. Toxicology tests of the pilot's liver fluid showed 0.345 mcg/ml codeine, 0.134 mcg/ml dextromethorphan, 0.249 mcg/ml dextrorphan, and an undetermined amount of morphine. A test of the pilot's blood indicated undetermined quantities of opiates, a class of drugs which includes codeine and morphine. Tests of kidney fluid showed 0.349 mcg/ml codeine, 0.027 mcg/ml dextromethorphan, and 0.191 mcg/ml dextrorphan. The finding of these substances is consistent with prior ingestion of codeine-containing cough syrup. Codeine, a narcotic pain reliever and cough suppressant, can produce impaired judgment, disorientation, and delayed reactions.
Probable Cause: failure of the pilot to maintain control of the airplane, due to spatial disorientation. Factors relating to the accident were: the pilot's use of an unapproved drug, low ceiling, restricted visibility (fog), and an undetermined anomaly with the vacuum system.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL97FA029 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB ATL97FA029
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 17:28 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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