ASN Wikibase Occurrence # 362047
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Date: | Monday 17 May 1993 |
Time: | 20:49 LT |
Type: | Beechcraft 36 |
Owner/operator: | M K F Flying Club, Inc. |
Registration: | N7687N |
MSN: | E-94 |
Year of manufacture: | 1968 |
Total airframe hrs: | 3440 hours |
Engine model: | CONTINENTAL IO-520-B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hayward, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | , CA (KHWD) |
Destination airport: | San Jose, CA (KSJC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT SAID HE TOOK OFF ON THE RIGHT FUEL TANK AND SWITCHED TO THE LEFT TANK AFTER LEVELING OFF AT 3,000 FEET. THE ENGINE QUIT JUST AFTER THE FUEL SELECTOR WAS TURNED. THE PILOT REPORTED THAT HE TURNED BACK TOWARD THE AIRPORT, SWITCHED FUEL TANKS AND ATTEMPTED TO RESTART THE ENGINE; HOWEVER, HE WAS UNABLE TO RESTORE POWER. THE AIRCRAFT COLLIDED WITH A DIRT BERM SHORT OF THE RUNWAY DURING THE ATTEMPTED POWER OFF FORCED LANDING. FAA AIRWORTHINESS INSPECTORS EXAMINED THE AIRCRAFT AND FOUND THAT THE RIGHT FUEL TANK WAS ABOUT HALF FULL AND THE LEFT TANK CONTAINED LESS THAN ONE GALLON. AFTER JACKING UP THE NOSE AND REPLACING THE PROPELLER, THE INSPECTOR RECONNECTED THE AIRCRAFT BATTERY, TURNED THE FUEL SELECTOR TO THE RIGHT TANK, AND STARTED THE ENGINE. DURING THE ENGINE RUN, ALL POWER PLANT GAUGES WERE READING IN NORMAL RANGES. FUEL SYSTEM CONTINUITY WAS ESTABLISHED THROUGHOUT THE AIRCRAFT. THE PILOT DID NOT SPECIFY HOW HE QUANTIFIED THE FUEL IN EACH TANK PRIOR TO DEPARTURE.
Probable Cause: fuel starvation due to the pilot's inadequate preflight inspection of the aircraft and his failure to ensure that adequate fuel existed in the fuel tanks to be used.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX93LA218 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB LAX93LA218
Revision history:
Date/time | Contributor | Updates |
17-Mar-2024 17:09 |
ASN Update Bot |
Added |
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