Accident Mooney M20C N6790V,
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ASN Wikibase Occurrence # 362539
 
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Date:Saturday 2 January 1993
Time:17:30 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20C
Owner/operator:Private
Registration: N6790V
MSN: 700084
Year of manufacture:1970
Total airframe hrs:3091 hours
Engine model:LYCOMING O-360-A1D
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Gorman, CA -   United States of America
Phase: En route
Nature:Private
Departure airport:Petaluma, CA (O69)
Destination airport:El Monte, CA (KEMT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE AIRPLANE WAS IN CRUISE FLIGHT AT ABOUT 9,500 FEET MEAN SEA LEVEL WHEN THE ENGINE HAD A TOTAL LOSS OF POWER. THE PILOT ENTERED A POWER OFF FORCED LANDING AND PERFORMED EMERGENCY PROCEDURES ATTEMPTING TO RE START THE ENGINE. HE COULD NOT GET THE ENGINE STARTED. THE PILOT LANDED THE AIRPLANE ON A TWO LANE ROAD ADJACENT TO AN INTERSTATE HIGHWAY. THE PILOT ENCOUNTERED AN UNFAVORABLE LEFT CROSSWIND WHICH CAUSED THE AIRPLANE TO DRIFT TO THE RIGHT SIDE OF THE ROAD. DURING LANDING ROLL THE AIRPLANE'S RIGHT WING CONTACTED METAL FENCE POSTS AND SPUN THE AIRPLANE INTO AN EMBANKMENT. DURING AN FAA SUPERVISED ENGINE RUN FUEL WAS NOTED AS LEAKING FROM THE CARBURETOR. AN EXAMINATION OF THE CARBURETOR REVEALED THAT THE INLET FUEL FITTING HAD GALLED OR CROSSFED THREADS. METAL SHAVINGS FROM THE THREADS BYPASSED THE FUEL SCREEN AND TRAVELED DIRECTLY INTO THE FUEL FLOAT VALVE WITHOUT GOING THROUGH THE FILTER SCREEN. THIS CAUSED THE FLOAT VALVE TO BECOME INOPERATIVE, WHICH RESULTED IN FLOODING THE ENGINE WITH FUEL CAUSING A TOTAL LOSS OF ENGINE POWER. THE AIRPLANE'S ENGINE HAD A TOTAL TIME OF 7 HOURS SINCE OVERHAUL.

Probable Cause: 1) THE CARBURETOR INLET FUEL LINE BEING IMPROPERLY INSTALLED BY MAINTENANCE PERSONNEL WHICH ALLOWED THE CARBURETOR TO BECOME CONTAMINATED WITH METAL PARTICLES, AND 2) THE CARBURETOR FLOAT VALVE BEING JAMMED BY METAL PARTICLES WHICH ALLOWED EXCESSIVE FUEL TO BE INTRODUCED INTO THE CARBURETOR RESULTING IN FLOODING AND THE TOTAL LOSS OF ENGINE POWER. A FACTOR IN THIS ACCIDENT WAS THE PILOT ENCOUNTERING AN UNFAVORABLE CROSSWIND DURING FINAL APPROACH WHICH LED TO THE AIRPLANE'S WING COLLIDING WITH FENCE POSTS DURING LANDING ROLL.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX93LA089
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB LAX93LA089

Location

Revision history:

Date/timeContributorUpdates
18-Mar-2024 07:31 ASN Update Bot Added

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