Accident Hughes 369D N113RS,
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ASN Wikibase Occurrence # 362581
 
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Date:Monday 21 December 1992
Time:16:00 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes 369D
Owner/operator:Mauna Kea Helicopters
Registration: N113RS
MSN: 590506D
Year of manufacture:1979
Total airframe hrs:6928 hours
Engine model:Allison 250 C20B
Fatalities:Fatalities: 0 / Occupants: 5
Aircraft damage: Substantial
Category:Accident
Location:Hilo, HI -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Kamuela, HI (MUE)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
DURING CRUISE THE PILOT DETECTED A BUFFETING IN THE AIRFRAME FOLLOWED BY A LEFT YAW. THE ENGINE GAGES INDICATED DECREASING POWER OUTPUT WITH A HIGH TURBINE OUTLET TEMPERATURE, AND, THE ENGINE CHIP AND FAILURE LIGHTS ILLUMINATED. THE PILOT EXECUTED AN AUTO ROTATION AND HAD TO STRETCH THE GLIDE SLIGHTLY TO REACH THE ONLY SUITABLE AREA WHICH INVOLVED A DOWN WIND LANDING. THE MAIN ROTOR SLICED OFF THE TAIL BOOM AS THE HELICOPTER SLID TO A STOP. REVIEW OF THE OPERATORS DAILY FLIGHT SHEETS FOR THE ACCIDENT HELICOPTER REVEALED THAT A ENGINE CHIP LIGHT HAD ILLUMINATED ON THE FLIGHT PRIOR TO THIS ONE. THE CORRECTIVE ACTION TAKEN WAS TO CLEAN THE CHIP PLUG AND REINSTALL IT. NO TEST FLIGHT AND FURTHER CHECK OF THE PLUG WAS DONE AS REQUIRED IN THE MAINTENANCE MANUALS. DISASSEMBLY OF THE ENGINE REVEALED THAT THE NUMBER 1 AND 2 BEARINGS IN THE COMPRESSOR MODULE HAD FAILED. REVIEW OF MAINTENANCE RECORDS REVEALED THAT THE COMPRESSOR MODULE WAS FORMERLY INSTALLED IN AN ENGINE WHICH WAS INVOLVED IN A HELICOPTER ACCIDENT IN MAY OF 1992. THE COMPRESSOR MODULE WAS NOT DISASSEMBLED FOR INSPECTION AS REQUIRED IN THE OVERHAUL AND MAINTENANCE MANUAL, AND WAS NOT SIGNED OFF FOR RETURN TO SERVICE. IT WAS INSTALLED BY THE OPERATOR IN THE ACCIDENT HELICOPTER ENGINE ON NOVEMBER 21, 1992.

Probable Cause: THE BEARING FAILURES DUE TO THE OPERATOR'S USE OF IMPROPER MAINTENANCE INSPECTION AND OVERHAUL PROCEDURES BY INSTALLING AN UNSERVICEABLE COMPRESSOR MODULE IN THE HELICOPTER ENGINE. FACTORS IN THE ACCIDENT WERE THE UNSUITABLE NATURE OF THE TERRAIN FOR THE FORCED LANDING AND THE TAIL WIND CONDITION DURING THE LANDING TOUCHDOWN.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX93LA071
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB LAX93LA071

History of this aircraft

Other occurrences involving this aircraft
25 March 1994 N113RS Mauna Kea Helicopters 0 Hi. Nat'l Park, HI sub
12 January 1999 C-GSSN Rupert's Land Operations 1 36 NM SW of Fox Creek, AB, Alberta unk
Fuel exhaustion

Location

Revision history:

Date/timeContributorUpdates
18-Mar-2024 08:07 ASN Update Bot Added

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