ASN Wikibase Occurrence # 36291
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 12 January 1990 |
Time: | 20:37 |
Type: | Cessna 182P Skylane |
Owner/operator: | private |
Registration: | N5831J |
MSN: | 18263559 |
Year of manufacture: | 1975 |
Total airframe hrs: | 3659 hours |
Fatalities: | Fatalities: 3 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Tom's Place, CA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Compton, CA (CPM) |
Destination airport: | Mammoth Lake, CA (MMH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT HAD A CABIN NR MAMMOTH/JUNE LAKES airport & OFTEN FLEW THERE ON WEEKENDS. THE PILOT HAD LANDED FOR A BRIEF STOP AT BIH AIRPORT PRIOR TO TAKING OFF AGAIN, CIRCLING THE OWENS VALLEY TO GAIN ALTITUDE, AND THEN PROCEDING NORTH TOWARD MMH.WHILE ON A NGT FLT, HE COMMUNICATED WITH AN OUTBOUND CARGO PLT, WHO WARNED OF HVY SNW FALL & POOR VIS AT THE ARPT. WHILE CONVERSING, THE PLT OF N5831J REPLIED, 'OH DEAR, MY CAR IS UP THERE.' THE CARGO PLT AGAIN WARNED THAT HE DOUBTED IF N5831J COULD LND AT THE ARPT. A WORKER, WHO LEFT THE airport AT 2030 PST, NOTED THE RWY LGTS CAME ON AS HE WAS DRIVING HOME. HE BELIEVED THE LGTS WERE ACTIVATED BY A PLT (BY KEYING THE MIKE 5 TIMES ON UNICOM FREQ). THREE WITNESSES SAW THE ACFT (OR ACFT LGTS) AT ABOUT THE TIME IT CRASHED. IMPACT OCCURRED IN A LEFT WING LOW, NOSE DWN ATTITUDE. ONE WITNESS THOUGHT THE ACFT WAS TURNING OR ARCING WHEN IT CRASHED. ANOTHER WITNESS ESTIMATED THERE WAS A 100' CEILING WITH SNW FALLING ON A DARK NGT. IMPACT WAS ABOUT 1 MI FM A HIWAY BTN MAMMOTH LAKES & BISHOP, CA (ABT 10 MI SE OF MAMMOTH/JUNE LAKES airport & 17 MI NW OF BISHOP ARPT). NO PREIMPACTPART FAILURE/MALFUNCTION OF THE ACFT OR ENG WAS FND. THERE WAS NO PUBLISHED INST APCH PROC AT MAMMOTH/JUNE LAKES ARPT. CAUSE: CONTINUED FLIGHT BY THE PILOT INTO INSTRUMENT METEOROLOGICAL CONDITIONS (IMC), AND HIS FAILURE TO MAINTAIN SUFFICIENT ALTITUDE ABOVE THE GROUND. FACTORS RELATED TO THE ACCIDENT WERE: DARK NIGHT, ADVERSE WEATHER CONDITIONS, SELF INDUCED PRESSURE, AND SPATIAL DISORIENTATION.
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001212X22402 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
11-Dec-2010 02:56 |
Robert Rasband |
Updated [Narrative] |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation