ASN Wikibase Occurrence # 363257
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 24 July 1992 |
Time: | 13:15 LT |
Type: | Mooney M20G |
Owner/operator: | Private |
Registration: | N6785N |
MSN: | 680095 |
Year of manufacture: | 1967 |
Total airframe hrs: | 2362 hours |
Engine model: | LYCOMING O-360-A1D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hendersonville, NC -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Savannah, GA (KSAV) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRPLANE LANDED, NOSE WHEEL FIRST, AT AN EXCESSIVE LANDING SPEED AND PORPOISED SEVERAL TIMES. A WITNESS STATED THAT WHEN THE AIRPLANE WAS ABOUT 500 FEET FROM THE END OF THE RUNWAY, THE LANDING WAS ABORTED. HIGH TREES BOUNDED THE DEPARTURE END OF THE RUNWAY. ACCORDING TO THE WITNESS THE AIRPLANE WAS UNABLE TO CLIMB OVER THE TREES AND STALLED. IT THEN COLLIDED WITH THE TREES & THE GROUND, WITH THE ENGINE AT 'FULL POWER.' THE AIRPLANE WAS FOUND IN A VERTICAL NOSE DOWN ATTITUDE. IT WAS SUPPORTED IN THAT POSITION BY THE THICK WOODS. THE PILOT SAID THAT THE ENGINE ACCELERATED WITHOUT HIS INPUT & THAT THE PROP GOVERNOR CABLE WAS FOUND BROKEN AT THE CONTROL PANEL END. THE PROP GOVERNOR ARM WAS FOUND IN THE FULL INCREASE POSITION. ADDITIONALLY, THE DENSITY ALTITUDE WAS CALCULATED TO BE 3500 FEET MSL.
Probable Cause: THE PILOT'S DELAY IN EXECUTING A RECOVERY FROM THE BOUNCED LANDING AND HIS INADVERTENT STALL DURING THE INITIAL CLIMB AFTER AND LANDING WAS ABORTED. FACTORS WERE THE EXCESSIVE LANDING SPEED AND THE HIGH DENSITY ALTITUDE.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL92LA144 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB ATL92LA144
History of this aircraft
Other occurrences involving this aircraft
16 May 2019 |
N3555N |
Private |
0 |
Bowling Green Municipal Airport (H19), Pike County, MO |
|
min |
Runway excursion |
Location
Revision history:
Date/time | Contributor | Updates |
18-Mar-2024 15:13 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation