Accident Beechcraft A36TC Bonanza N206WJ,
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ASN Wikibase Occurrence # 36357
 
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Date:Sunday 19 September 1999
Time:12:58 LT
Type:Silhouette image of generic BT36 model; specific model in this crash may look slightly different    
Beechcraft A36TC Bonanza
Owner/operator:Terry L. Barrett
Registration: N206WJ
MSN: EA-206
Total airframe hrs:4766 hours
Engine model:Continental TSIO-520-UB
Fatalities:Fatalities: 4 / Occupants: 4
Aircraft damage: Destroyed
Category:Accident
Location:Franklinton, LA -   United States of America
Phase: En route
Nature:Private
Departure airport:Baton Rouge, LA (BTR
Destination airport:Montgomery, AL
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported to ATC that 'he wanted to come down to the nearest airport due to an cylinder overheating problem.' The pilot was vectored to an airport with a 3,000 foot runway. A witness observed the airplane 'high and fast' as it entered the pattern. Witnesses observed the airplane flying over runway 31 with the landing gear extended, at 15 to 35 feet agl. Witnesses reported the airplane assumed a nose high attitude as 'if the airplane was attempting to climb,' and subsequently, they heard the sound of the engine increase. One of the witnesses reported 'the engine sounded as if it was flooded or bogged down.' The pilot lost control of the airplane as he attempted to clear trees at the departure end of the runway. The gear was found in the 'in-transit' position with the wing flaps fully extended. Examination of the engine revealed a hole eroded through the side of the piston for the #2 cylinder. Both spark plugs for the #2 cylinder were found filled with aluminum debris around their electrodes. Examination of the propeller indicated that it was being operated with low power at the time of impact.

Probable Cause: The pilot's inadvertent stall while attempting to clear trees during a go-around. Factors were the pilot's misjudgment of the airplane's distance and speed during the precautionary landing and the partial loss of engine power due to a perforated piston.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW99FA262
Status: Investigation completed
Duration: 1 year and 10 months
Download report: Final report

Sources:

NTSB FTW99FA262

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
14-Dec-2017 09:04 ASN Update Bot Updated [Operator, Source, Narrative]
07-Apr-2024 17:52 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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