ASN Wikibase Occurrence # 363724
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 26 April 1992 |
Time: | 16:30 LT |
Type: | Cessna 177RG |
Owner/operator: | Private |
Registration: | N33248 |
MSN: | 177RGO932 |
Engine model: | LYCOMING IO-360-A1B6D |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mammoth Lakes, CA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | (KMMH) |
Destination airport: | Burbank, CA (KBUR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:BEFORE TAKEOFF, THE PLT RECEIVED A WX BRIEFING & A LOCAL AUTOMATED WX OBSERVATION THAT REPORTED STANDING LENTICULAR CLOUDS & 9100' DENSITY ALTITUDE. HE TOOK OFF ON RWY 27, WHICH SLOPED UPWARD & WAS SURROUNDED BY MOUNTAINOUS TERRAIN. THE WIND WAS REPORTEDLY FROM 270 DEG AT 4 GUSTING 18 KTS & THE ACFT WAS LOADED AT/NEAR ITS MAXIMUM TAKEOFF WT. THE PLT SAID THAT FOR TAKEOFF, THE MIXTURE WAS SET FOR 'HIGHEST RPM AND PEAK EGT,' BUT THE FLT MANUAL RECOMMENDED THE MIXTURE BE LEANED ACCORDING TO THE MAXIMUM POWER FUEL FLOW PLACARD. AFTER LIFT-OFF, THE PLT HAD DIFFICULTY ESTABLISHING A CLIMB. HE SAID THE ACFT WOULD NOT CLIMB AFTER REACHING 500' AGL & BEGAN LOSING ALTITUDE. A PASSENGER SAID THE PLT CIRCLED & TRIED TO GAIN ALTITUDE, BUT ENCOUNTERED A DOWNDRAFT. REPORTEDLY, THE STALL WARNING HORN SOUNDED ALMOST CON- TINUOUSLY. THE PLT SAID HE TURNED BACK TOWARD THE AIRPORT, BUT THE DESCENT INCREASED. SUBSEQUENTLY, HE LANDED SHORT OF RWY 27 & THE ACFT HIT DITCHES DURING THE LANDING ROLL. THE ENG WAS NOT DAMAGED & WAS RETURNED TO SVC WITHOUT REPAIR.
Probable Cause: THE PILOT-IN-COMMAND'S INACCURATE WEATHER EVALUATION, HIS IMPROPER SETTING OF THE MIXTURE CONTROL, AND HIS FAILURE TO MAINTAIN PROPER CLIMB AIRSPEED. FACTORS RELATED TO THE ACCIDENT WERE: HIGH DENSITY ALTITUDE, UNFAVORABLE WIND WITH MOUNTAIN WAVE ACTIVITY AND DOWNDRAFTS, THE PILOT'S APPARENT LACK OF EXPERIENCE WITH THE TYPE OF OPERATION (MOUNTAIN FLYING), AND DITCHES IN THE EMERGENCY LANDING AREA.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX92LA190 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB LAX92LA190
Location
Revision history:
Date/time | Contributor | Updates |
18-Mar-2024 20:21 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation