Serious incident Boeing 727-214A N752US,
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ASN Wikibase Occurrence # 363814
 
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Date:Sunday 9 February 1992
Time:19:10 LT
Type:Silhouette image of generic B722 model; specific model in this crash may look slightly different    
Boeing 727-214A
Owner/operator:USAir
Registration: N752US
MSN: 21691/1480
Year of manufacture:1979
Total airframe hrs:35403 hours
Engine model:P&W JT8D-15A
Fatalities:Fatalities: 0 / Occupants: 157
Aircraft damage: Minor
Category:Serious incident
Location:San Juan -   Puerto Rico
Phase: Initial climb
Nature:Unknown
Departure airport:
Destination airport:Philadelphia, PA (PHL
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
FLT LOST 'A' HYDRAULIC SYSTEM WHEN LEFT MAIN GEAR DOOR UP LINE RUPTURED DURING GEAR RETRACTION AT POINT IT HAD CHAFFED ON APU. CAPT CALLED FOR 30,000 POUNDS OF FUEL TO BE DUMPED FOLLOWED BY MANUAL EXTENSION OF THE LANDING GEAR. FLT ENG COULD NOT GET RT MAIN GEAR TO EXTEND MANUALLY. CAPT TOLD FLT ENG TO VIEW POSITION OF MAIN LANDING GEAR THROUGH VIEW PORTS IN CABIN. FLT ENG COULD NOT LOCATE THE VIEW PORTS AND RETURNED TO COCKPIT. CAPT THEN ORDERED FUEL DUMPED TO MINIMUM LEVEL AFTER WHICH A LANDING WITH RT MAIN GEAR RETRACTED WAS MADE. AFTER LANDING WHEN AIRCRAFT WAS RAISED THE RT MAIN LANDING GEAR WAS FOUND TO BE STOWED ON THE UPLOCK NORMALLY. THE GEAR WAS THEN EXTENDED FOLLOWING NORMAL MANUAL EXTENSION PROCEDURES. NO EVIDENCE OF MALFUNCTION OF THE RT MAIN GEAR WAS FOUND. THE RT MAIN GEAR EXTENDS BY CRANKING OPPOSITE DIRECTION FROM THE LEFT AND NOSE GEAR. THE FLT ENG BECAME QUALIFIED AS FLT ENG ON 11/03/91 AND HAD ACCUMULATED 200 HOURS AS FLT ENG.

Probable Cause: THE FLIGHT ENGINEER'S LACK OF TRAINING IN EMERGENCY PROCEDURES AND HIS FAILURE TO FOLLOW PUBLISHED EMERGENCY PROCEDURES, RESULTING IN HIS NOT BEING ABLE TO MANUALLY EXTEND THE RIGHT MAIN LANDING GEAR, FOLLOWING THE LOSS OF THE 'A' HYDRAULIC SYSTEM. CONTRIBUTING TO THE INCIDENT WAS THE CAPTAINS FAILURE TO EXHAUST ALL AVAILABLE RESOURCES AND TIME IN ATTEMPTS TO EXTEND THE RIGHT MAIN LANDING GEAR PRIOR TO LANDING WITH THE GEAR RETRACTED.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA92IA081
Status: Investigation completed
Duration: 1 year and 4 months
Download report: Final report

Sources:

NTSB MIA92IA081

History of this aircraft

Other occurrences involving this aircraft
13 January 1999 N785AT American Trans Air 0 New York-La Guardia Airport, NY (LGA/KLGA) non

Revision history:

Date/timeContributorUpdates
19-Mar-2024 06:24 ASN Update Bot Added

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