ASN Wikibase Occurrence # 363996
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Date: | Sunday 1 March 1992 |
Time: | 14:09 LT |
Type: | Cessna 402C |
Owner/operator: | Airways International |
Registration: | N6786C |
MSN: | 402C0413 |
Year of manufacture: | 1980 |
Total airframe hrs: | 11498 hours |
Engine model: | CONTINENTAL TSIO-520-VB |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Fort Lauderdale, FL -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Miami, FL (KMIA) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE NOSE LANDING GEAR COLLAPSED AFTER IT WAS LOWERED TO THE RWY DURING THE LANDING ROLL. EXAM OF THE NOSE LANDING GEAR ASSY BY AN FAA MAINTENANCE INSPECTOR INDICATED THAT THE NOSE LANDING GEAR ACTUATOR WAS NOT DAMAGED. IT WAS REMOVED FOR EXAM. DISASSEMBLY REVEALED THAT AN EXTRA PACKING (SIMILAR TO AN O-RING) WAS INSTALLED. THIS ALLOWED THE NOSE LANDING GEAR DOWN AND LOCKED LIGHT TO ILLUMINATE BUT SHUT THE MOTOR OFF BEFORE THE NOSE LANDING GEAR WAS FULLY EXTENDED. REVIEW OF THE AIRPLANE LOGBOOKS INDICATE THAT A PROGRESSIVE INSPECTION WAS SIGNED OFF TWO DAYS BEFORE THE ACCIDENT. DURING THE INSPECTION IT WAS NOTED THAT THE NOSE LANDING GEAR ACTUATOR SWITCH WAS LEAKING. THE CORRECTIVE ACTION INDICATES THAT THE O-RINGS WERE REPLACED. ACCORDING TO THE ILLUSTRATED PARTS LIST OF THE NOSE LANDING GEAR ACTUATOR, TWO PACKINGS ARE INSTALLED. ACCORDING TO THE DIRECTOR OF MAINTENANCE, THE MECHANIC RESPONSIBLE FOR REPLACEMENT OF THE PACKINGS WAS PROVIDED WITH TWO, BUT ONLY REMOVED ONE FROM THE ACTUATOR. THIS RESULTED IN THE EXTRA PACKING. THE ACFT HAD ACCUMULATED 4 HRS & 6 CYCLES SINCE THE INSPECTION 2 DAYS EARLIER.
Probable Cause: IMPROPER OVERHAUL BY COMPANY MAINTENANCE PERSONNEL AND INACCURATE GEAR DOWN AND LOCKED INDICATION IN THE COCKPIT.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA92IA090 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB MIA92IA090
History of this aircraft
Other occurrences involving this aircraft
13 July 2003 |
N314AB |
Air Sunshine |
2 |
7,35 nm WNW of Treasure Cay Airport (MYAT) |
|
w/o |
Location
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 08:20 |
ASN Update Bot |
Added |
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