Accident Beechcraft A36 N88ES,
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ASN Wikibase Occurrence # 364051
 
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Date:Saturday 25 January 1992
Time:15:25 LT
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36
Owner/operator:Loren Kula, Et Al
Registration: N88ES
MSN: E-758
Year of manufacture:1975
Total airframe hrs:5878 hours
Engine model:CONTINENTAL IO-520-BB12
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Albuquerque, NM -   United States of America
Phase: Landing
Nature:Private
Departure airport:Bullhead City, AZ (P06
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE AIRPLANE WAS DAMAGED WHEN IT COLLIDED WITH ROUGH, SOFT TERRAIN AND THE GEAR COLLAPSED DURING A FORCED LANDING ON A DIRT ROAD. THE FORCED LANDING WAS EXECUTED FOLLOWING A POWER LOSS DUE TO FUEL EXHAUSTION WHILE THE AIRPLANE WAS DESCENDING TO LAND AT ITS DESTINATION. NO FUEL WAS FOUND IN THE SYSTEM FOLLOWING THE ACCIDENT AND NO FUEL STAINS WERE FOUND ON THE AIRPLANE. THE PIC STATED THAT THE ESTIMATED TIME EN ROUTE HAD EXTENDED FROM TWO HOURS AND FORTY FIVE MINUTES TO THREE HOURS AND THIRTY SIX MINTES, BUT THAT THE FUEL GAUGES READ EMPTY AND ONE QUARTER FULL WHEN HE ARRIVED IN THE AREA OF HIS DESTINATION. THE PILOT STATED THAT HE THOUGHT THAT HE HAD A HANGING MAIN GEAR DOOR AND IT CREATED A LOW PRESSURE AREA NEAR THE FUEL TANK VENTS WHICH PRESSURIZED THE FUEL TANKS AND CAUSED SIPHONING. THE FUEL CONSUMPTION RATE FOR THE OUTBOUND FLIGHT HAD BEEN 12.3 GPH AND THE RETURN FLIGHT FUEL CONSUMPTION WAS 15.8 GPH AT, ACCORDING TO THE PILOT, THE SAME POWER SETTINGS.

Probable Cause: THE PILOT IN COMMAND FAILED TO PROPERLY MONITOR THE FUEL CONSUMPTION RATE OF THE AIRPLANE WHEN HE PERCEIVED THAT IT MIGHT BE HIGHER THAN NORMAL. THE ENGINE FAILURE WAS A RESULT OF FUEL EXHAUSTION, AGGRAVATED BY POSSIBLE FUEL SIPHONING FROM THE TANKS.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW92LA060
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB FTW92LA060

Location

Revision history:

Date/timeContributorUpdates
19-Mar-2024 08:53 ASN Update Bot Added

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