ASN Wikibase Occurrence # 364087
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 12 January 1992 |
Time: | 10:40 LT |
Type: | Cessna 172N |
Owner/operator: | K & M Aviation |
Registration: | N1571E |
MSN: | 17271049 |
Year of manufacture: | 1978 |
Total airframe hrs: | 9000 hours |
Engine model: | LYCOMING O-320-H2AD |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Show Low, AZ -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Phoenix, AZ (KDVT) |
Destination airport: | Albuquerque, NM |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT SAID WHILE IN LEVEL CRUISE ON AN IFR FLIGHT THE ENGINE BEGAN TO LOOSE POWER DUE TO CARBURETOR ICE AND ATTEMPTS TO REMEDY THE SITUATION WERE UNSUCCESSFUL WITH THE ENGINE EVENTUALLY LOOSING ALL POWER. THE PILOT DECLARED AN EMERGENCY WITH ALBUQUERQUE CENTER AND WAS RADAR VECTORED TOWARD THE SHOW LOW AIRPORT. THE FLIGHT WAS INTERMITTENTLY IN CLOUDS DURING THE EMERGENCY DESCENT AND BROKE OUT AT A LOW ALTITUDE. THE AIRCRAFT HAD INSUFFICIENT ALTITUDE TO MAKE THE AIRPORT AND LANDED IN THE ONLY AVAILABLE LOCATION, A FIELD ABOUT 23 MILES FROM THE AIRPORT. DURING ROLL OUT, THE AIRCRAFT COLLIDED WITH A DITCH AND NOSED OVER. POST ACCIDENT EXAMINATION OF THE AIRCRAFT BY FAA INSPECTORS REVEALED THAT THE CARBURETOR HEAT BOX HAD SEPARATED FROM THE HEAT MUFF OF THE EXHAUST SYSTEM AND WAS HANGING LOOSE IN THE COWLING ATTACHED ONLY BY THE FABRIC HOSE. A METAL BAND WHICH ATTACHES THE CARB HEAT BOX TO THE MUFF HAD SEPARATED. CHAFFING ON THE COWLING IN THE AREA OF WHERE THE HEAT BOX WAS HANGING INDICATED IT HAD BEEN SEPARATED FOR SOME TIME. THE LAST 100 HOUR INSPECTION WAS ACCOMPLISHED 80 OPERATING HOURS PRIOR TO THE ACCIDENT.
Probable Cause: THE FAILURE OF THE CARBURETOR HEAT BOX ATTACH STRAPS WHICH ALLOWED THE CARBURETOR HEAT BOX TO SEPARATE FROM THE EXHAUST SYSTEM HEAT MUFF AND RENDERED THE CARBURETOR HEAT SYSTEM INOPERATIVE. THE ENGINE THEN LOST POWER DUE TO CARBURETOR ICE.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX92LA089 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB LAX92LA089
Location
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 09:18 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation