ASN Wikibase Occurrence # 36423
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Date: | Saturday 18 December 1999 |
Time: | 10:17 LT |
Type: | Velocity 173 RG Elite |
Owner/operator: | Kenneth W. Swertfeger |
Registration: | N627KB |
MSN: | DMO 375 |
Total airframe hrs: | 87 hours |
Engine model: | Lycoming IO-360-C1C6 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Murfreesboro, TN -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Decatur, AL (KDCU) |
Destination airport: | (KMBT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was on approach for landing when the airplane experienced a total loss of engine power, and crashed during a forced landing. Examination of the airframe and engine assembly revealed no evidence of a precrash mechanical failure or malfunction. Visual inspection of the spark plugs revealed very black and sooty. Fuel was present in the flow divider but was not present in the line between the fuel servo and flow divider. The servo fuel injector was removed and examined. The fuel diaphragm had not been replaced. The servo fuel injector was placed in a test bench and a functional test performed. Fuel was pouring out of the venturi causing erratic air flow through the regulator and erratic air flow. The air cover and diaphragm was removed to determine the source of the fuel leak. The fuel diaphragm stem was bent. The center body was removed with the fuel diaphragm attached to the center body bellows. The bottom calibration nut was removed from the fuel diaphragm stem. The fuel diaphragm was removed from the bellows and a leakage check was performed. The bellows was split and air was leaking through the bellows. Appropriate AD's and SB's had not been complied with resulting in an in-flight power loss due to an over rich condition.
Probable Cause: The failure of an unknown maintenance person to comply with an Airworthiness Directive (replace center body bellows seal assembly and tube bushings) and Service Bulletin (replace fuel diaphragm) resulting in an in-flight power loss due to an over rich condition caused by the failure of the center body bellows seal assembly, and subsequent forced landing and in-flight collision with terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA00LA053 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB MIA00LA053
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
15-May-2010 11:01 |
JINX |
Updated [Aircraft type, Source] |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Dec-2017 10:00 |
ASN Update Bot |
Updated [Cn, Operator, Destination airport, Source, Narrative] |
07-Apr-2024 16:10 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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