ASN Wikibase Occurrence # 364301
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Date: | Monday 28 October 1991 |
Time: | 08:05 LT |
Type: | McDonnell Douglas DC-10-10 |
Owner/operator: | United Airlines |
Registration: | N1820U |
MSN: | 46619/119 |
Total airframe hrs: | 50708 hours |
Engine model: | GE CF 6-6 |
Fatalities: | Fatalities: 0 / Occupants: 179 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Las Vegas, NV -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Los Angeles, CA (KLAX) |
Destination airport: | Denver, CO (KDEN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE CLIMBING THRU 35,000 FT FOR A CRUISE ALTITUDE OF 37,000 FT, THE CREW HEARD A LOUD 'THUMP' & THE ACFT DEPRESSURIZED. AS THE CREW DESCENDED TO 11,000 FT, THE CABIN ALTITUDE CLIMBED TO 30,000 FT. THE FLT DIVERTED TO A NEARBY ARPT & SAFELY LANDED. EXAM OF THE ACFT DISCLOSED THAT REPETITIVE PRESSURIZATION CYCLES CAUSED THE INITIATION OF A FATIGUE CRACK & THE RESULTANT RUPTURE OF A FORWARD PRESSURE BULKHEAD. OVER 14 YRS EARLIER, DOUGLAS ISSUED SERVICE BULLETINS ADVISING OPERATORS THAT LEAKS COULD OCCUR IN THE FWD PRESSURE BULKHEAD AREA BECAUSE OF METAL FATIGUE. DOUGLAS RECOMMENDED THAT SPECIFIC CORRECTIVE ACTION BE TAKEN WHICH INVOLVED INSPECTING THE AREA AT 1,500 HOUR INTERVALS OR MAKING PERMANENT STRUCTURAL AIRFRAME MODIFICATIONS. CONTRARY TO THE MAJORITY OF ACFT OPERATORS, UNITED CHOSE NOT TO STRUCTURALLY MODIFY THIS ACFT. RATHER, IT CHOSE TO PERFORM RECURRING VISUAL INSPECTIONS FOR LEAKS IN THE SUSPECT AREA. THE ACFT'S PRESSURE BULKHEAD RUPTURED 1,367 HRS AFTER IT LAST INSPECTION.
Probable Cause: RUPTURE OF A FORWARD PRESSURE BULKHEAD BECAUSE OF CYCLICALLY INDUCED METAL FATIGUE. FACTORS WHICH CONTRIBUTED TO THE INCIDENT WERE: THE OPERATOR'S DECISION NOT TO STRUCTURALLY MODIFY ITS AIRPLANE IN ACCORDANCE WITH THE MANUFACTURER'S BUT RATHER TO RELY ON THE MANUFACTURER'S ALTERNATIVE RECOMMENDATION OF PERFORMING REPETITIVE VISUAL INSPECTION IN THE SUSPECT AREA: AND THE OPERATOR'S FAILURE TO UTILIZE AN INSPECTION PROGRAM ADEQUATE TO VISUALLY DETECT CRACK DEVELOPMENT IN A PREVIOUSLY IDENTIFIED SUSPECT AREA.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX92IA027 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB LAX92IA027
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 13:42 |
ASN Update Bot |
Added |
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