ASN Wikibase Occurrence # 364919
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Date: | Sunday 14 July 1991 |
Time: | 14:05 LT |
Type: | Bell 206B |
Owner/operator: | Houston Helicopters, Inc. |
Registration: | N16962 |
MSN: | 2362 |
Year of manufacture: | 1978 |
Total airframe hrs: | 7336 hours |
Engine model: | Allison 250-C20B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Freeport, TX -
United States of America
|
Phase: | Landing |
Nature: | Ferry/positioning |
Departure airport: | Pearland, TX (NONE) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT STATED THAT THE FUEL GAUGE READ 74 GALLONS DURING HIS PRE FLIGHT INSPECTION AND THAT 10 MINUTES AFTER TAKEOFF, WHEN HE WAS ABOUT HALF WAY TO HIS DESTINATION, IT WAS READING 24 GALLONS. HE FURTHER STATED THAT WHEN HE WAS ABOUT 5 MILES FROM THE DESTINATION THE BOOST PUMP LIGHTS CAME ON AND THE GAUGE WAS READING 5 GALLONS. HE STATED THAT AT THAT POINT HE DECIDED TO EXECUTE A PRECAUTIONARY LANDING AND FIND THE PROBLEM. THE ENGINE FLAMED OUT DUE TO FUEL EXHAUSTION BEFORE HE COULD LAND AND HE ENTERED AUTOROTATION. DURING THE DESCENT THE PILOT NOTICED THAT HE WAS GOING TO HIT A BUSH AND HE EXTENDED HIS GLIDE OVER THE BUSH. AS A RESULT THE AIRCRAFT LANDED HARD IN A TAIL LOW ATTITUDE. INVESTIGATION REVEALED THAT THE PILOT HAD NOT VISUALLY CHECKED THE FUEL DURING THE PRE FLIGHT AND THAT THE AIRCRAFT HAD 20 GALLONS OF FUEL ON BOARD WHEN HE DEPARTED ON THE ACCIDENT FLIGHT. ALL OF THE FUEL SYSTEM COMPONENTS, INCLUDING THE FUEL GAUGE WERE FUNCTIONALLY TESTED AND OPERATED NORMALLY.
Probable Cause: THE PILOT'S FAILURE TO MAINTAIN SUFFICIENT ROTOR RPM DURING THE AUTOROTATION. FACTORS WERE THE FUEL EXHAUSTION INDUCED POWER LOSS DUE TO THE PILOT'S IMPROPER PRE-FLIGHT INSPECTION.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW91LA121 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB FTW91LA121
History of this aircraft
Other occurrences involving this aircraft
15 November 2002 |
N16962 |
John McCoy |
1 |
Kingman, AZ |
|
sub |
Collision with pole or wires |
Location
Revision history:
Date/time | Contributor | Updates |
19-Mar-2024 20:16 |
ASN Update Bot |
Added |
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