ASN Wikibase Occurrence # 365155
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 10 June 1991 |
Time: | 23:30 LT |
Type: | Cessna 172M |
Owner/operator: | Raleigh East Airport |
Registration: | N12498 |
MSN: | 17262022 |
Engine model: | LYCOMING O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Knighdale, NC -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Goldsboro, NC (GWW |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AFTER PERFORMING A GO-AROUND, THE PILOT INITIATED A SECOND APPROACH TO LAND AT NIGHT. ON SHORT FINAL, HE INADVERTENTLY ACCELERATED THE AIRPLANE, AND IT BEGAN TO BALLOON ABOVE THE RUNWAY. THE AIRPLANE LANDED LONG AND OVERRAN THE RUNWAY. SUBSEQUENTLY, IT COLLIDED WITH TWO AUTOMOBILES AND A PARKED AIRPLANE, THEN IT HIT A DITCH. THE PILOT STATED THAT THE ACCIDENT WOULD HAVE BEEN AVOIDED IF HE HAD PERFORMED A GO-AROUND INSTEAD OF TRYING TO SALVAGE THE LANDING.
Probable Cause: FAILURE OF THE PILOT TO ATTAIN THE PROPER TOUCH DOWN POINT ON THE RUNWAY AND/OR PERFORM A GO-AROUND.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL91LA109 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB ATL91LA109
Location
Revision history:
Date/time | Contributor | Updates |
20-Mar-2024 07:10 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation