ASN Wikibase Occurrence # 365712
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Date: | Tuesday 5 February 1991 |
Time: | 03:10 LT |
Type: | Piper PA-60-600 |
Owner/operator: | Top Flight Inc. |
Registration: | N6070D |
MSN: | 600677961214 |
Engine model: | LYCOMING IO-540-S1A5 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Cochran, GA -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Atlanta, GA (KATL) |
Destination airport: | Tampa, FL (KTPA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE CRUISING AT 7000 FEET THE PILOT EXPERIENCED A LOSS OF POWER ON THE RIGHT ENGINE. THE PILOT REQUESTED ASSISTANCE FROM JACKSONVILLE CENTER, AND WAS VECTORED TO COCHRAN AIRPORT. THE PILOT ESTABLISHED AN APPROACH TO THE AIRPORT BUT WAS UNABLE TO LOWER THE WING FLAPS. APPARENTLY, AFTER THE LANDING GEAR WAS EXTENDED, THERE WAS NOT ENOUGH HYDRAULIC PRESSURE AVAILABLE TO LOWER THE WING FLAPS. THE ONLY HYDRAULIC PUMP WAS INSTALLED ON THE RIGHT ENGINE. THE PILOT LOST DIRECTIONAL CONTROL DURING THE LANDING ROLLOUT, AND THE AIRPLANE VEERED OFF THE RIGHT SIDE OF THE RUNWAY INTO A DITCH. THE PILOT STATED THAT HEAVY LEFT BRAKING WAS USED, BUT FAILED TO CORRECT THE RIGHTWARD DRIFT. ACCORDING TO THE FLIGHT MANUAL, THE PILOT SHOULD USE ENGINE POWER AND BRAKING TO MAINTAIN DIRECTIONAL CONTROL DURING THE EMERGENCY LANDING. EXAMINATION OF THE AIRPLANE DISCLOSED THAT THE RIGHT FUEL SHUTOFF VALVE HAD FAILED AND FUEL WAS SHUTOFF TO THE RIGHT ENGINE. ADDITIONALLY, THE RIGHT WING SPAR WAS REPAIRED PRIOR TO RESTORING THE AIRPLANE TO A FULL AIRWORTHY STATUS.
Probable Cause: FAILURE OF THE RIGHT ENGINE SHUTOFF VALVE WHICH RESULTED IN A COMPLETE LOSS OF ENGINE POWER. THE AIRPLANE VEERED OFF THE RIGHT SIDE OF THE RUNWAY AND THE RIGHT MAIN LANDING GEAR COLLAPSED AS A RESULT OF THE PILOTS FAILURE TO MAINTAIN DIRECTIONAL CONTROL DURING THE LANDING ROLLOUT. FACTORS IN THIS INCIDENT WERE THE DARK NIGHT, AND A LOSS OF HYDRAULIC PRESSURE WHEN THE RIGHT ENGINE FAILED.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL91IA050 |
Status: | Investigation completed |
Duration: | 2 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB ATL91IA050
Location
Revision history:
Date/time | Contributor | Updates |
20-Mar-2024 13:00 |
ASN Update Bot |
Added |
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