Accident Mooney M20C N1389W,
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ASN Wikibase Occurrence # 366073
 
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Date:Sunday 7 October 1990
Time:12:30 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20C
Owner/operator:Private
Registration: N1389W
MSN: 2667
Total airframe hrs:2316 hours
Engine model:LYCOMING O-360-A1D
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Kissimmee, FL -   United States of America
Phase: En route
Nature:Private
Departure airport:Stuart, FL (KSUA)
Destination airport:Toccoa, GA (KTOC)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE PLT RPRTD THE ENG STARTED & RAN NORMALLY BEFORE TAKEOFF. HOWEVER, DURING FLT, IT BEGAN RUNNING ROUGH. THE PLT REDUCED THE POWER SETTING WHICH INITIALLY ELIMINATED THE ENG ROUGHNESS. HE CHECKED EACH MAGNETO & NOTED NO MALFUNCTION; HOWEVER, WHILE DIVERTING TO A NEARBY ARPT, THE ENG AGAIN BEGAN RUNNING ROUGH & A SEVERE LOSS OF POWER OCCURRED. ACCORDING TO WITNESSES, THE ACFT STRUCK A PALM TREE DURING A LEFT DESCENDING TURN AT LOW ALTITUDE & CRASHED. THE ENG WAS EQUIPPED WITH BENDIX MODEL S4LN-200 SERIES MAGNETOS. DURING A BENCH CHECK BOTH MAGNETOS BEGAN MISFIRING AFTER ABOUT 15 TO 20 MIN OF OPN. DISASSEMBLY OF THE MAGNETOS REVEALED THE NONCONDUCTIVE MATERIAL IN THE COILS WAS CRACKED & WAS BEGINNING TO LIQUEFY; THIS RESULTED IN MISDIRECTION OF THE HIGH VOLTAGE SPARK. THE MAGNETOS HAD APRX 2316 HRS IN SVC. ACCORDING TO AD 73-07-04, THE COILS IN THE MAGNETOS OF THIS ACFT SHOULD HAVE BEEN REPLACED AFTER ACCUMULATING APRX 2000 HRS OF OPN. THE ACFT HAD FLOWN 11 HRS SINCE THE LAST ANNUAL INSPN.

Probable Cause: MALFUNCTION OF BOTH MAGNETOS DUE TO DETERIORATION OF THE COILS, FAILURE OF MAINTENANCE PERSONNEL TO COMPLY WITH AN AIRWORTHINESS DIRECTIVE, AND FAILURE OF THE PILOT TO MAINTAIN ADEQUATE VISUAL LOOKOUT WHILE ON AN APPROACH FOR AN EMERGENCY LANDING. FACTORS RELATED TO THE ACCIDENT WERE: THE OBSTRUCTION (TREE) IN THE EMERGENCY LANDING AREA, AND DIVERSION OF THE PILOT'S ATTENTION WHILE APPROACHING TO LAND.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA91FA008
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB MIA91FA008

Revision history:

Date/timeContributorUpdates
20-Mar-2024 17:07 ASN Update Bot Added

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