ASN Wikibase Occurrence # 366408
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Date: | Tuesday 7 August 1990 |
Time: | 12:30 LT |
Type: | Aerospatiale SA 315B Lama |
Owner/operator: | Pegasus Helicopters, Inc. |
Registration: | N58000 |
MSN: | 2639 |
Total airframe hrs: | 3607 hours |
Engine model: | TURBOMECA ARTOUSTE IIIB |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tok, AK -
United States of America
|
Phase: | Taxi |
Nature: | Unknown |
Departure airport: | Tok, AK (TKJ) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE HELICOPTER WAS BEING USED IN AN EXTERNAL LOAD OPN TO CARRY CARGO WITH A 100 FT CABLE. WHILE HOVERING OUT OF GROUND EFFECT, THE ENG LOST PWR. A SUBSEQUENT HOVERING AUTOROTATION RESULTED IN A HARD LANDING. AN EXAM REVEALED THE LOSS OF POWER WAS DUE TO FUEL CONTAMINATION ALTHOUGH AN AIRFRAME FUEL FILTER WAS INSTALLED IN THE MAIN FUEL SUPPLY LINE. AN EXAM REVEALED THE FILTER ELEMENT HAD BEEN INSTALLED BACKWARD IN THE FILTER CANISTER. THIS ALLOWED CONTAMINATED FUEL TO BYPASS THE FILTER ELEMENT & ENTER THE ENG FUEL CTL UNIT. THE REVERSE INSTLN ALSO RESULTED IN AN INOP 'FUEL FILTER CLOGGED' WARNING LGT & PREVENTED THE PRESSURE DIFFERENTIAL BUTTON ON THE FILTER HOUSING FM EXTDG. THE FILTER HAD BEEN INSPECTED & REINSTLD DRG A 100 HR INSPN, 17 FLT HRS BFR THE ACDNT. THIS WORK WAS DONE BY A PLT UNDER SUPERVISION OF A MECHANIC. THE MECHANIC HAD NO PREV EXPERIENCE WITH THIS MAKE & MODEL OF HELICOPTER. 'TOP' & 'BOTTOM' WERE STENCILED ON THE FILTER ELEMENT IN FRENCH. CONTAMINATED FUEL WAS ALSO FND IN THE FUEL TRUCK.
Probable Cause: IMPROPER INSTALLATION OF THE FUEL FILTER ELEMENT IN THE AIRCRAFT BY COMPANY/MAINTENANCE PERSONNEL, AND SUBSEQUENT CONTAMINATION OF THE FUEL SYSTEM BY UNFILTERED FUEL. FACTORS RELATED TO THE ACCIDENT WERE: INADEQUATE DESIGN OF THE FUEL FILTER ASSEMBLY, WHICH ALLOWED THE IMPROPER INSTALLATION OF THE FILTER ELEMENT, THE MECHANICS LACK OF FAMILIARITY WITH THE AIRCRAFT, AND FAILURE OF GROUND PERSONNEL TO INSURE THAT FUEL FROM THE FUEL TANKER WAS FREE OF CONTAMINATION.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC90LA135 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB ANC90LA135
History of this aircraft
Other occurrences involving this aircraft
28 July 1996 |
C-FSWN |
Hi-Wood Helicopters Ltd. |
0 |
Cranbrook, British Columbia |
|
unk |
Location
Revision history:
Date/time | Contributor | Updates |
20-Mar-2024 20:44 |
ASN Update Bot |
Added |
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