ASN Wikibase Occurrence # 366587
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Date: | Saturday 14 July 1990 |
Time: | 14:30 LT |
Type: | Mooney M20F |
Owner/operator: | B & L Aviation, Inc. |
Registration: | N6456Q |
MSN: | 670535 |
Year of manufacture: | 1967 |
Total airframe hrs: | 5740 hours |
Engine model: | LYCOMING IO-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Torrington, WY -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (KTOR) |
Destination airport: | Rapid City, SD (KRAP) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PRIVATE PILOT TOOK OFF AND ATTEMPTED TO CLIMB. HE SAID THE ENGINE SEEMED TO BE PRODUCING ONLY PARTIAL POWER. HE TURNED BACK TO THE RUNWAY, BUT LOST ALTITUDE, DRAGGED ONE WING ON THE TERRAIN, AND LANDED ACROSS THE 75 FOOT WIDE RUNWAY. THE PLANE CROSSED THE RUNWAY, A TAXIWAY, SKIDDED UP A HILL AND CAME TO REST. THE FUSELAGE, BOTH WINGS, THE NOSE GEAR AND LEFT MAIN GEAR WERE DAMAGED. A POSTACCIDENT INVESTIGATION REVEALED A BROKEN EXHAUST VALVE IN THE NUMBER ONE CYLINDER.
Probable Cause: A PARTIAL LOSS OF POWER DUE TO A FAILED EXHAUST VALVE. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN90LA164 |
Status: | Investigation completed |
Duration: | 2 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB DEN90LA164
Location
Revision history:
Date/time | Contributor | Updates |
21-Mar-2024 10:04 |
ASN Update Bot |
Added |
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