ASN Wikibase Occurrence # 367342
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 4 March 1990 |
Time: | 12:19 LT |
Type: | Piper PA-28-151 |
Owner/operator: | Private |
Registration: | N991DB |
MSN: | 28-7615424 |
Year of manufacture: | 1976 |
Total airframe hrs: | 4356 hours |
Engine model: | LYCOMING O-320-E3D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Creola, AL -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PRIVATE PILOT WAS TEST FLYING AN AIRPLANE FOLLOWING A NUMBER THREE CYLINDER CHANGE. ON INITIAL CLIMB, THE ENGINE BEGAN TO VIBRATE, BACKFIRE AND LOSE POWER. THE AIRPLANE CRASHED ON A HIGHWAY MEDIAN LOCATED ABOUT ONE MILE FROM THE AIRPORT CENTER. A POST-CRASH INSPECTION OF THE ENGINE REVEALED A PIECE OF EXHAUST VALVE LODGED IN THE NUMBER ONE PISTON HEAD. ANOTHER VALVE FRAGMENT WAS FOUND INSIDE THE MUFFLER. THE PILOT REPORTED THAT THE NUMBER THREE CYLINDER CHANGE WAS THE RESULT OF A PREVIOUSLY FAILED NUMBER THREE EXHAUST VALVE AND SUBSEQUENT INTERNAL DAMAGE TO THE NUMBER THREE CYLINDER. AN ASSUMPTION WAS MADE THAT THE FRAGMENTS FROM THE FAILED VALVE HAD EXITED THE ENGINE VIA THE EXHAUST SYSTEM. A LOCAL MECHANIC CHANGED THE CYLINDER, BUT DID NOT COMPLETE THE REPAIR DUE TO A LACK OF TIME. THE PILOT FINISHED THE REPAIR, TEST RAN THE ENGINE, AND FLEW THE AIRPLANE ON THE ACCIDENT FLIGHT. THE ENGINE WAS NOT CERTIFIED AIRWORTHY PRIOR TO THE FLIGHT.
Probable Cause: THE PILOT'S FAILURE TO ASSURE THAT PROPER MAINTENANCE AND INSPECTION OF THE AIRCRAFT WERE COMPLETED BEFORE FLIGHT.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL90FA071 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB ATL90FA071
Location
Revision history:
Date/time | Contributor | Updates |
22-Mar-2024 13:18 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation