Accident Eurocopter-Kawasaki BK-117B-2 N370SS,
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ASN Wikibase Occurrence # 368657
 
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Date:Friday 13 May 2022
Time:21:00
Type:Silhouette image of generic BK17 model; specific model in this crash may look slightly different    
Eurocopter-Kawasaki BK-117B-2
Owner/operator:Mercy Flight Central Holding LLC
Registration: N370SS
MSN: 7133
Year of manufacture:1987
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Strong Memorial Hospital Heliport (2NY5), Rochester, NY -   United States of America
Phase: Standing
Nature:Ambulance
Departure airport:Strong Memorial Hospital Heliport, NY (2NY5)
Destination airport:Strong Memorial Hospital Heliport, NY (2NY5)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On May 13, 2022, about 2100 eastern daylight time, a Messerschmitt-Bolkow-Blohm BK117 B-2 helicopter, N370SS, was substantially damaged when it was involved in an accident at the Strong Memorial Hospital Heliport, Rochester, New York. The commercial pilot and two crewmembers were not injured. The helicopter was operated as a Title 14 Code of Federal Regulations Part 135 air ambulance flight.

After the pilot of the air medical helicopter landed, the medical crew boarded and he prepared the helicopter for takeoff. The pilot stated that he was adjusting a light switch while his right hand was on the cyclic control when he heard a loud “bang.” He subsequently noticed that the rod from the airframe-mounted wire cutter was bouncing back and forth. The pilot then shut down the engines and the crew exited the helicopter. A postaccident examination of the helicopter revealed substantial damage to the main rotor blades that was consistent with them having contacted the wire cutter. The examinations otherwise did not reveal evidence of any anomalies of the flight control system that would have precluded normal operation. Based on this information, while the pilot indicated that he was holding the cyclic control at the time of the event, given the damage to the helicopter and the lack of anomalous findings with the flight control system, nor the existence other external influences like substantive wind, it is likely that he inadvertently moved the cyclic, which resulted in the main rotor briefly moving into a position where it contacted the wire cutter.

Probable Cause: An unintentional movement of the cyclic control before takeoff, which resulted the main rotor blades contacting the fixed wire cutter.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: 
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB

https://data.ntsb.gov/Docket?ProjectID=105085

Location

Revision history:

Date/timeContributorUpdates
23-Mar-2024 22:45 Captain Adam Added

Corrections or additions? ... Edit this accident description

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