ASN Wikibase Occurrence # 368954
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 9 April 1989 |
Time: | 18:02 LT |
Type: | Cessna 152 |
Owner/operator: | Barlett Aviation Inc. |
Registration: | N25884 |
MSN: | 15280831 |
Year of manufacture: | 1977 |
Total airframe hrs: | 3636 hours |
Engine model: | LYCOMING O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Irwindale, CA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Training |
Departure airport: | El Monte, CA (KEMT) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A CESSNA 152 COLLIDED WITH A FENCE DURING A FORCED LANDING. AT 4,000 FT MSL, THE CFI SWITCHED THE FUEL SHUT OFF VALVE TO THE OFF POSITION TO SIMULATE AN ENG FAILURE. THE STUDENT PILOT SWITCHED THE FUEL SHUT OFF VALVE TO THE ON POSITION. THE ENG DID NOT REGAIN RPM. THE CFI THEN 'DOUBLE CHECKED' TO SEE THAT THE STUDENT SWITCHED THE FUEL SHUT OFF VALVE TO THE 'ON' POSITION. THE ENG BEGAN TO FIRE AND THEN QUIT. THE CFI THEN CHECKED THE FUEL SHUT OFF VALVE AGAIN ALONG WITH THE MIXTURE CTRL, MAGNETOS, AND ENG PRIMER. AT 2000 FT MSL THE PROPELLER STOPPED TURNING. THE CFI ENGAGED THE STARTER IN AN ATTEMPT TO RESTART THE ENG. THE CFI OVERSHOT THE INTENDED LANDING AREA AND SELECTED ANOTHER ROAD AND LANDED SHORT OF IT. THE ACFT STRUCK A FENCE AND NOSED OVER. THE ACFT WAS EXAMINED AND THE CARBURETOR FUEL BOWL WAS FOUND EMPTY OF FUEL. AC 61-21 STATES, IN PART, 'THE CFI SHOULD GIVE SIMULATED FORCED LANDINGS BY RETARDING THE THROTTLE.'
Probable Cause: IMPROPER PROCEDURE USED BY THE CERTIFIED FLIGHT INSTRUCTOR IN SIMULATING AN ENGINE FAILURE. CONTRIBUTING TO THIS ACCIDENT WAS THE LACK OF TOTAL FLIGHT INSTRUCTION EXPERIENCE OF THE FLIGHT INSTRUCTOR.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX89LA155 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB LAX89LA155
Location
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 09:15 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation