ASN Wikibase Occurrence # 368978
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Date: | Wednesday 5 April 1989 |
Time: | 14:27 LT |
Type: | Bell 206B |
Owner/operator: | Industrial Helicopters |
Registration: | N5004L |
MSN: | 2451 |
Year of manufacture: | 1978 |
Total airframe hrs: | 6728 hours |
Engine model: | Allison 250-C20B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | West Cameron, -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE HELICOPTER HAD SVRL INFLT ENG DECELERATIONS THAT MAINTENANCE EFFORTS DID NOT ISOLATE. AFTER REPLACING THE ENG FUEL CONTROLLER, A TEST FLT WAS MADE (FROM AN OIL DRILLING PLATFORM). DRG THE FLT, THE ENG SURGED, THEN DECELERATED. THE PLT WAS UNABLE TO REACH THE HELIPAD. HE ELECTED TO LAND ON THE PLATFORM, SHORT OF THE HELIPAD, RATHER THAN ACCEPT SEA CONDS OF 8 FT WAVES. DRG THE LANDING, THE HELICOPTER WAS DAMAGED. A POST-ACDNT EXAM REVEALED FUEL CONTAMINATION HAD OCCURRED. CONTAMINATION HAD BYPASSED FILTERS IN THE FUEL SYS & HAD CLOGGED & COLLAPSED THE ENG FUEL NOZZLE SCREEN. THE AIRFRAME FUEL FILTER CAP BYPASS VLV WAS FND STUCK OPEN IN THE BYPASS MODE. A PIN (CONNECTED TO THE FUEL FILTER CAP IMPENDING BYPASS TEST BUTTON) WAS FND BENT, HOLDING THE BYPASS VLV OPEN. AN OPEN BYPASS VLV SHOULD HAVE ILLUMINATED A RESPECTIVE ANNUNCIATOR LIGHT IN THE COCKPIT; HOWEVER, WHEN CHECKED, THE ANNUNCIATOR LIGHT OPERD ONLY INTERMITTENTLY DUE TO A FAULTYCOMPONENT IN THE SYS. DRG TESTS, THE CLOGGED/COLLAPSED FUEL SCREEN PREVENTED SUFFICIENT FUEL FLOW TO SUSTAIN ENG POWER.
Probable Cause: INADEQUATE MAINTENANCE/INSPECTION OF THE AIRCRAFT FUEL SYSTEM BY COMPANY MAINTENANCE PERSONNEL AND FUEL CONTAMINATION, WHICH RESULTED IN A PARTIAL LOSS OF ENGINE POWER. RELATED FACTORS WERE: A BINDING (STUCK) FUEL FILTER CAP BYPASS VALVE AND PARTIAL FAILURE (INTERMITTENT OPERATION) OF THE RESPECTIVE ANNUNCIATOR LIGHT SYSTEM.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW89FA075 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB FTW89FA075
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 09:33 |
ASN Update Bot |
Added |
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