ASN Wikibase Occurrence # 369560
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 9 November 1988 |
Time: | 18:52 LT |
Type: | Cessna 152 |
Owner/operator: | Gator Air |
Registration: | N6578B |
MSN: | 15283954 |
Total airframe hrs: | 3825 hours |
Engine model: | LYCOMING O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gainesville, FL -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT TAXIED TO RWY 6 & MADE AN ENG RUN-UP. AS HE CALLED THE TWR FOR TKOF, A NAVY P-3 WAS MAKING A LOW APCH TO RWY 10.THE PLT WAS TOLD TO TAXI TO RWY 10. ABT 30 SEC LATER, AS HE ARRIVED AT RWY 10, HE WAS CLRD FOR TKOF & WAS CAUTIONED ABT WAKE TURBC FM THE P-3. THE PLT TKOF ON RWY 10 & MNVRD TO AVOID WAKE TURBC. AS THE ACFT WAS CLIMBING THRU ABT 100', IT ROLLED VIOLENTLY TO THE RGT. THE PLT APPLIED CORRECTIVE ACTION, BUT THE ACFT DSCNDD & HIT THE RWY BFR HE COULD RCVR. THEAIM & FAA ADZY CIRCULAR 90-23D WARNED OF WAKE TURBC & RCMDD 2 MIN INTERVAL WHEN SMALL ACFT IS DEPG BHND A LARGE ACFT. THE TWR CTLR COMPLIED WITH APPLICABLE ATC DIRECTIVES. PARAGRAPH 3-106I OF ATC HANDBOOK 7110.65F SAID TO 'SEPARATE A SMALL ACFT BHND A LARGE ACFT TAKING OFF OR MAKING A LOW/MISSED APCH WHEN UTILIZING OPPOSITE DRCTN TAKEOFFS ON THE SAME RWY BY 3 MIN UNLESS A PLT HAS INITIATED A REQUEST TO DEVIATE FM THE 3 MIN INTERVAL. IN THE LATTER CASE, ISSUE A WAKE TURBC ADZY BEFORE CLRG THE ACFT FOR TAKEOFF.' HOWEVER, THE HANDBOOK DID NOT ADDRESS TAKEOFFS BHND SAME DRCTN LOW APCHS.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA89LA022 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB MIA89LA022
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 15:54 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation