ASN Wikibase Occurrence # 369645
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 18 October 1988 |
Time: | 09:25 LT |
Type: | Cessna 150F |
Owner/operator: | Private |
Registration: | N8194F |
MSN: | 15064294 |
Year of manufacture: | 1966 |
Total airframe hrs: | 2520 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Goodyear, AZ -
United States of America
|
Phase: | Landing |
Nature: | Executive |
Departure airport: | Tucson, AZ (KRYN) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT RPRTD THAT DRG THE LANDING ROLL, THE ACFT ENCTRD A GUST OF WIND & VEERED OFF THE DIRT STRIP & ONTO A RAISED BERM (EDGE OF RWY). AFTER ENCTRG THE SOFT DIRT & ROUGH TERRAIN, THE NOSE GEAR COLLAPSED & THE PLANE NOSED OVER. THE PLT HAD LANDED WITH 40 DEG OF FLAPS. HE ESTIMATED THE WIND WAS FROM 240 DEG AT 6 GUSTING TO 18 KTS. NO PRE-ACDNT MECHANICAL MALFUNCTION OR FAILURE OF THE ACFT WAS RPRTD.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX89LA017 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB LAX89LA017
Location
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 16:47 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation