ASN Wikibase Occurrence # 369804
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Date: | Friday 16 September 1988 |
Time: | 16:10 LT |
Type: | Bell 206L |
Owner/operator: | Kenai Air Of Hawaii Inc |
Registration: | N278KA |
MSN: | 46613 |
Year of manufacture: | 1978 |
Total airframe hrs: | 10395 hours |
Engine model: | Allison 250-C20B |
Fatalities: | Fatalities: 0 / Occupants: 7 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lihue, HI -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING A LOCAL SIGHTSEEING FLIGHT, THE PILOT REPORTED THAT WHILE ON FINAL APPROACH FOR LANDING, THE AUDIO AND LIGHT FOR LOW RPM SOUNDED AND ILLUMINATED. THE HELICOPTER WAS AUTOROTATED. IT INITIALLY BOUNCED WHEN IT TOUCHED DOWN, THEN LANDED HARD. THE ENGINE WAS STILL RUNNING AFTER THE ACCIDENT. THE ENGINE WAS REMOVED AND PLACED ON A TEST CELL. ALL ENGINE PARAMETERS EXCLUDING THE SEAL VENT PRESSURE, WERE FOUND TO BE WITHIN LIMITS AS RECOMMENDED BY THE MANUFACTURER. AFTER CHANGING THE VENT ORIFICE FROM A NO. 2 TO A NO. 4 THE DISCREPANCY WAS CORRECTED.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX88LA325 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB LAX88LA325
Location
Revision history:
Date/time | Contributor | Updates |
24-Mar-2024 18:25 |
ASN Update Bot |
Added |
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