Serious incident McDonnell Douglas DC-10-30 N270AX,
ASN logo
ASN Wikibase Occurrence # 370256
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Wednesday 2 May 2007
Time:11:06 LT
Type:Silhouette image of generic DC10 model; specific model in this crash may look slightly different    
McDonnell Douglas DC-10-30
Owner/operator:Omni Air International
Registration: N270AX
MSN: 48318/446
Total airframe hrs:39144 hours
Engine model:General Electric CF6-50C2
Fatalities:Fatalities: 0 / Occupants: 306
Aircraft damage: None
Category:Serious incident
Location:Atlanta, GA -   United States of America
Phase: Unknown
Nature:Passenger - Non-Scheduled/charter/Air Taxi
Departure airport:Shannon Airport (SNN/EINN)
Destination airport:Atlanta Hartsfield-Jackson International Airport, GA (ATL/KATL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While flying at 13,000 feet mean sea level (msl), and decelerating to 250 knots in a DC-10-30 airplane, the horizontal stabilizer could not be moved by either commands from the autopilot or using the primary and alternate control switches from the cockpit. The horizontal stabilizer remained at approximately 1 degree airplane nose-up which resulted in excessive cockpit control forces. An emergency was declared with air traffic control and the flight landed uneventfully on runway 27R at ATL. The inoperative horizontal stabilizer trim system was caused by improper overhaul of the horizontal stabilizer chain drive unit drive assembly (horizontal stabilizer drive assembly) P/N AJH 7337-507, S/N DCA-418 by omission of one pin (P/N 3D0009-5-4), one nut (P/N MS21043-08), and one washer (P/N NAS 1252-BL) which secure the drive gear of the horizontal stabilizer drive assembly. The omission of the parts resulted in fatigue failure of another pin (P/N AJH7378-1) and shear failure of the single installed pin (P/N 3D0009-5-4). This prevented output of the horizontal stabilizer drive assembly being transmitted to acme screws of the horizontal stabilizer. There was no flight crew write-ups for the previous 93 days related to pitch trim. The horizontal stabilizer drive assembly was overhauled on April 30, 1999, and installed in the incident airplane on April 23, 2006. The airplane had accumulated 2,421 hours and 473 cycles since the overhauled assembly was installed.

Probable Cause: The improper overhaul of the horizontal stabilizer chain drive unit drive assembly.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA07IA088
Status: Investigation completed
Duration: 1 year and 9 months
Download report: Final report

Sources:

NTSB MIA07IA088

Location

Revision history:

Date/timeContributorUpdates
25-Mar-2024 08:43 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org