Serious incident Hughes 369D N58267,
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ASN Wikibase Occurrence # 370310
 
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Date:Friday 14 October 2005
Time:11:13 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes 369D
Owner/operator:Alexair
Registration: N58267
MSN: 390473D
Year of manufacture:1979
Total airframe hrs:24575 hours
Engine model:Rolls-Royce 250-C20B
Fatalities:Fatalities: 0 / Occupants: 5
Aircraft damage: Minor
Category:Serious incident
Location:Kahului, HI -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Kahului Airport, HI (OGG/PHOG)
Destination airport:Kahului Airport, HI (OGG/PHOG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The helicopter was damaged during a hard landing following a loss of tail rotor control. The pilot was conducting a tour flight when tail rotor control was lost. He conducted an emergency landing and landed hard when the helicopter encountered a gust of wind. Examination of the tail rotor system revealed that the tail rotor control rod failed about 6.5 inches forward of its aft attach point, where the control rod attaches to the tail rotor pitch change bell crank. The control rod fractured perpendicular to its longitudinal axis and displayed a flat fracture surface. Metallurgical examination of the control rod fracture revealed that it failed as a result of fatigue cracking that propagated from the outside in. The crack origin could not be determined due to severe mechanical damage from relative movement between the fracture mating surfaces. Due to the damage, the size of the crack could not be determined, and therefore, an assessment of the crack's age could not be made. As a result, it was not possible to determine whether or not the crack would have been visible during the last inspection, which took place 91.2 hours prior to the accident. That inspection's checklist called for the removal and inspection of the tail rotor control rod.

Probable Cause: The fatigue cracking and failure of the tail rotor control rod during cruise flight, which resulted in a hard landing during the precautionary landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX06IA011
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report

Sources:

NTSB LAX06IA011

Location

Revision history:

Date/timeContributorUpdates
25-Mar-2024 09:21 ASN Update Bot Added

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