Serious incident Beechcraft 1900D N136MJ,
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ASN Wikibase Occurrence # 370314
 
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Date:Tuesday 2 August 2005
Time:17:09 LT
Type:Silhouette image of generic B190 model; specific model in this crash may look slightly different    
Beechcraft 1900D
Owner/operator:Colgan Air. Inc
Registration: N136MJ
MSN: UE-36
Year of manufacture:1992
Total airframe hrs:20535 hours
Engine model:Pratt & Whitney PT6A-67D
Fatalities:Fatalities: 0 / Occupants: 9
Aircraft damage: None
Category:Serious incident
Location:Rockland, ME -   United States of America
Phase: Take off
Nature:Unknown
Departure airport:Rockland-Knox County Regional Airport, ME (RKD/KRKD)
Destination airport:Augusta State Airport, ME (AUG/KAUG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During the takeoff rotation, the captain pulled the yoke with both hands, but it did not move. The captain then pulled significantly harder, and the yoke moved quickly aft. The airplane jumped into the air, but the captain was able to maintain controlled flight, and continue to the destination airport. During cruise flight, everything was normal except that the elevator trim moved slowly nose up, which required an input of 1/2-unit nose down trim every 1 to 2 minutes. Subsequent examination of the airplane revealed that the left elevator could be moved around by hand. Further examination revealed that seven rivets were loose, and one rivet was missing in the vicinity of the left side elevator outer hinge-point attach bracket. Ground tests were unable to duplicate the elevator anomaly as reported by the captain. However, a fleet inspection of the operator's aircraft revealed that five of the eleven airplanes had loose rivets on the elevator hinge-point attach brackets. In addition, fleet inspections of other operators' same make and model aircraft revealed that some of the airplanes had loose rivets on the elevator hinge-point attach brackets. The suspect rivets and elevator were replaced on the incident airplane, and the anomaly did not reoccur.

Probable Cause: A loose elevator attachment, which resulted in a partial elevator binding during takeoff and uncommanded elevator movement during cruise.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC05IA128
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB NYC05IA128

Location

Revision history:

Date/timeContributorUpdates
25-Mar-2024 09:22 ASN Update Bot Added

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