Runway incursion Serious incident Boeing 737-7H4 N461WN,
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ASN Wikibase Occurrence # 370348
 
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Date:Thursday 19 August 2004
Time:14:55 LT
Type:Silhouette image of generic B737 model; specific model in this crash may look slightly different    
Boeing 737-7H4
Owner/operator:Southwest Airlines
Registration: N461WN
MSN: 32465/1510
Year of manufacture:2004
Total airframe hrs:1080 hours
Engine model:General Electric CFM-56
Fatalities:Fatalities: 0 / Occupants: 142
Aircraft damage: None
Category:Serious incident
Location:Los Angeles International Airport, CA (LAX/KLAX) -   United States of America
Phase: Standing
Nature:Passenger - Scheduled
Departure airport:Los Angeles International Airport, CA (LAX/KLAX)
Destination airport:Albuquerque International Airport, NM (ABQ/KABQ)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Asiana Airlines flight 204 (AAR204), a Boeing 747-400 that had been cleared to land on runway 24L, initiated a go-around and overflew Southwest Airlines flight 440 (SWA440), a Boeing 737 which had been cleared into position and hold for takeoff on runway 24L. Radar reconstruction of the event found that AAR204 passed over SWA440 at 200 feet during the go-around. At the time of the incident, a controller change for the LC2 position had just occurred and the relief controller was responsible for the air traffic control handling of both AAR204 and SWA440.

At 2151:21, the LC2 controller who was being relieved cleared AAR204 to land runway 24L. At this point, the Boeing 747 was 9.3 miles from the runway. About 2 minutes later, while AAR204 proceeded inbound on the approach, the LC2 controller provided a relief briefing to the LC2 relief controller and advised him that AAR204 was landing on runway 24L, which the relief controller acknowledged. After assuming the responsibility of the position, the first transmission from the LC2 relief controller was to SWA440 instructing the flight crew to taxi into position and hold on runway 24L. AAR204 was 1.81 miles from the runway at 700 feet. According to the SWA440 captain's statement, he saw the Asiana Boeing 747 on final approach but believed that the aircraft was landing on runway 24R. Twelve seconds later, the relief controller cleared SWA440 for takeoff. Radar data indicated AAR204 was 1.26 miles from the runway and about 35 seconds from reaching the landing threshold. Data retrieved from the SWA440's flight data recorder indicated the airplane was on taxiway V approaching runway 24L when given the takeoff clearance. This meant that the flight crew had less than 35 seconds to taxi on to runway 24L, begin a departure roll, and travel 6,000 feet before AAR440 crossed the landing threshold, which would be impossible. According to the Asiana captain's statement, he observed the Southwest Boeing 737 approaching runway 24L but believed the airplane would hold short of the runway. Once he recognized the aircraft was entering the runway, he initiated a go-around and estimated it was about the time his airplane was passing through 400 feet approaching the runway.

The relief controller said that contrary to the recorded relief briefing where he clearly acknowledged that AAR204 was cleared for the left runway, he fully believed AAR204 was landing runway 24R, and therefore, was unaware of the conflict. He first became aware of the problem when the Airport Movement Area Safety System (AMASS) generated an alarm. At this point, AAR440 was only about 12 seconds from colliding with SWA440, and without the prompt actions of the Asiana flight crew a collision would have likely occurred. When the relief controller recognized the problem, he canceled SWA440's takeoff clearance and AAR440's landing clearance. However, AAR204 had already overflown SWA440 on the go-around, clearing the aircraft by about 200 feet. Although the relief controller believed AAR204 was landing runway 24R, this did not alleviate his responsibility to properly monitor the operation and ensure separation was maintained.

Recorded voice communications of the position relief briefing indicated the LC2 controller informed the relief controller that the inboard runway (RWY 24L) was in use for landings, and that AAR204 was cleared to land on runway 24L. There was no indication from the relief controller that he did not understand or needed clarification from the relieving controller. The LC2 controller addressed all major areas on the LAX position relief checklist, and conveyed information accurately during the position relief briefing. About 30 seconds after the LC2 controller completed the briefing, he remembered additional information about helicopter operations and began relating that to the relief controller; however, this conversation was interrupted by another radio transmission, which effectively distracted both the LC2 controller and relief controller and likely exacerbated the difficulty the relief controller had in converting the briefing information in his short term memory to working memory. Immediately following the relief briefing, the LC2 controller left the postion.

Based on what is known about the volatility of information held in short term memory, and the speed of decay in short term memory without rehearsal of the information, it is not surprising that the relief controller failed to recall every detail LC2 controller's position relief briefing with complete accuracy. The relief controller was briefed on the location and clearances for seven aircraft (seven pieces of information is about the limit that can be effectively retained short term memory), but was not given sufficient opportunity to rehearse this information in working memory until 13 seconds after the briefing was completed. The format and timing of the position relief briefing and its interruption by routine radio transmissions contributed to the relief controller's memory error.

LAX tower controllers interviewed during the investigation stated that, because of the location of the tower, it was difficult to determine visually whether a single approaching aircraft was lined up for runway 24R or runway 24L. Controllers stated that destination runways were most difficult to determine visually for large aircraft, such as the Boeing 747. The LC2 relief controller believed this was the reason he did not recognize the conflict between AAR204 and SWA440. Although this may be true, it does not alleviate the controller of his responsibility to monitor the operation. In addition, the relief controller was aware the inboard runways were in use for landings and should have been alert to the possibility of aircraft arriving on runway 24L.

To assist the controllers with visual observations, the LAX tower is equipped with Digital Bright Radar Indicator Terminal Equipment (DBRITE) displays. The relief controller stated that he saw AAR204's radar target on the DBRITE display during the position relief briefing, but that he did not specifically recall seeing AAR204's data block. A review of the radar replay indicated AAR204's data block displayed two sets of alternating aircraft information: runway assignment and aircraft type were presented for 5 seconds; followed by a 15-second presentation of altitude and ground speed data. The relief controller stated that he glanced at his DBRITE display before the runway incursion. However, he clearly did not perceive the critical information that AAR204 was assigned to land on runway 24L, and he therefore did not take action to eliminate the conflict. Time-sharing of runway assignment information on the aircraft data tag increased the likelihood that critical information would not be perceived when parallel approaches were being conducted on the north side of the LAX tower.

LAX is equipped with (Airport Movement Area Safety System) AMASS, which is a computer software enhancement to the airport surface detection equipment. The LAX AMASS at the LC2 position generated an aural and visual alert only 12 seconds before a collision would have occurred, warning the controller to the impeding conflict; however, the flight crew of AAR204 had observed the Southwest Boeing 737 taxing towards the runway and, believing the aircraft was not going to stop, initiated a go-around before the AMASS alert activated. A collision was avoided, not by AMASS, but by the actions of the flight crew of AAR204.

At the time of the incursion, five certified professional controllers and one operations supervisor were working in the tower cab. According to facility personnel, there would normally be 10 people available to work on this shift but injuries and illness had reduced the available shift staff to five. It is common for ATC to combine positions to accommodate facility and/or operational needs. Controllers routinely work combined positions and are specifically trained to do so. However, in this situation, the absence of a local assist controller eliminated an additional safety net established to assist local controllers. The staffing decisions made by the Federal Aviation Administration supervisor on duty at the time of the incursion decreased the likelihood that the relief controller's error would be detected and corrected prior to the runway incursion.

In its evaluation of fatigue, the investigation determined that the relief controller had only 8 hours off between the end of his August 18 evening shift at 2330, and the beginning of his morning shift at 0730 on the day of the accident. As a result, the relief controller reported sleeping just "5 or 6 hours" the night before the incursion, and described his shift leading up to the incursion as a "hard day." This acute sleep loss resulted in a slight decrease in cognitive performance on tasks involving working memory and reaction time.

Probable Cause: a loss of separation between Southwest flight 440 and Asiana flight 204 due to the LC2 relief controller's failure to appropriately monitor the operation and recognize a developing traffic conflict. Contributing factors included the FAA's position relief briefing procedures, the formatting of the DBRITE radar displays in the LAX tower, controller fatigue, and the tower supervisor's staffing decisions on the day of the incident.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX04IA302
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB LAX04IA302

Location

Revision history:

Date/timeContributorUpdates
25-Mar-2024 09:42 ASN Update Bot Added

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