ASN Wikibase Occurrence # 370432
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Date: | Thursday 5 September 2002 |
Time: | 07:40 LT |
Type: | Fokker 100 |
Owner/operator: | American Airlines |
Registration: | N1473K |
MSN: | 11515 |
Year of manufacture: | 1994 |
Total airframe hrs: | 20571 hours |
Engine model: | Rolls-Royce 850-15 |
Fatalities: | Fatalities: 0 / Occupants: 33 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Minneapolis, MN -
United States of America
|
Phase: | Take off |
Nature: | Unknown |
Departure airport: | Minneapolis-St. Paul International Airport, MN (MSP/KMSP) |
Destination airport: | Chicago-O'Hare International Airport, IL (ORD/KORD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During takeoff the #2 wheel separated from the left main landing gear assembly. A company mechanic stated that during a walk-around inspection he noted the #1 and #2 main landing gear tires needed to be replaced. The #1 & #2 tires are on the left main landing gear assembly; with the #1 tire being outboard of the #2 tire. The mechanic reported, "We removed & replaced #2 main landing gear [tire], with nothing unusual during the tire change." The axle nut/spacer assembly was found with the wheel. The axle nut lock-bolts were found installed in the axle nut/spacer assembly with safety wire connecting the lock-bolts to the axle nut. The lock-bolts were not damaged. The interfacing threads between the axle nut/spacer assembly and the axle were not stripped and the treads were not worn. A demonstration of a wheel installation and a review of the installation procedures were performed at the request of the NTSB. In order for the lock-bolts to engage the axle keyslot, the axle nut/spacer assembly had to be properly torqued and wheel bearings seated.
Probable Cause: The improper installation of the #2 main landing gear wheel, including the axle nut not being properly torqued and safetied, which resulted in the wheel separation during takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI02IA270 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB CHI02IA270
Location
Revision history:
Date/time | Contributor | Updates |
25-Mar-2024 10:40 |
ASN Update Bot |
Added |
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