ASN Wikibase Occurrence # 370435
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Date: | Monday 26 August 2002 |
Time: | 21:35 LT |
Type: | MBB BK-117 A4 |
Owner/operator: | Rocky Mountain Helicopters |
Registration: | N528SF |
MSN: | 7104 |
Year of manufacture: | 1986 |
Engine model: | Lycoming LTS-101-650 |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Bradenton, FL -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Naples, FL |
Destination airport: | St. Petersburg, FL |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot said that while in cruise flight at an altitude of 1,000 feet, a speed of about 130 knots, and about 60 percent torque, without warning he heard a loud explosion from the right side of the helicopter, with simultaneous No. 2 engine fire and failure warning lights and indications, along with severe vibrations. He said that the helicopter yawed several times from left to right and he heard a "whopping" sound. He also said that at the same time the No. 1 engine torque meter needle moving rapidly from about the 9 to 3 or 4 o'clock positions on the gauge. The investigation revealed two of the power turbine blades and four rear bearing support housing (RBSH) failed in overload. The hub had been displaced from the engine centerline, and a deflection had occurred at the engine case axial midpoint, along with a misalignment of the inlet housing and the rear bearing support housing (RBSH). The resultant damage to the gas producer (GP) system, was consistent with an assembly error and mechanical failure having occurred by the loss of critical internal operating clearances and radial support for the rotors. Continued engine operation as the failure progressed led to compressor surge and the emergence of combustion gases from the No. 2 engine inlet, which ignited inlet cowling material. The No. 1 engine ingested smoke and combustion by-products from the engine cowling fire which caused a temporary stall condition.
Probable Cause: Improper maintenance/installation of the No. 2 engine power turbine (PT) wheel assembly by company maintenance personnel, which resulted in deflection at the engine case axial midpoint and misalignment between the inlet housing and the rear bearing support housing (RBSH) which resulted in damage to the engine and an in-flight fire.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA02IA160 |
Status: | Investigation completed |
Duration: | 2 years and 5 months |
Download report: | Final report |
|
Sources:
NTSB MIA02IA160
Location
Revision history:
Date/time | Contributor | Updates |
25-Mar-2024 10:41 |
ASN Update Bot |
Added |
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