ASN Wikibase Occurrence # 370759
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 7 July 1988 |
Time: | 19:05 LT |
Type: | Grumman G-164 Ag-Cat |
Owner/operator: | T And R Ag Service |
Registration: | N6848K |
MSN: | 503B |
Year of manufacture: | 1978 |
Engine model: | P&W R-1340-AN1 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Baker, MO -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Agricultural |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WITNESSES SAID THAT SHORTLY AFTER TAKEOFF, THE FULLY LOADED ACFT APPEARED TO BE UNABLE TO CLIMB OUT OF GROUND EFFECT. ABOUT 1.5 MILE FROM THE AIRSTRIP, THE PILOT BEGAN A TURN BACK TO THE NORTH. UNABLE TO CLIMB, HE INITIATED ACTION TO DUMP HIS CHEMICAL LOAD, BUT WAS UNABLE TO CLEAR POWER LINES. SUBSEQUENTLY, THE ACFT CRASHED INVERTED IN A FLOODED RICE FIELD. ABOVE NORMAL TEMP & HUMIDITY RESULTED IN AN ABOVE NORMAL DENSITY ALTITUDE. WITNESSES RPRTD THE ENG SOUNDED NORMAL DURING FLT. THE PLT SUFFERED TOXIC CHEMICAL CONTAMINATION & WAS TAKEN TO A HOSPITAL FOR TREATMENT. NO POWERPLANT OR CONTROL SYSTEM MALFUNCTION WAS FOUND.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC88LA129 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB MKC88LA129
Location
Revision history:
Date/time | Contributor | Updates |
25-Mar-2024 14:39 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation