ASN Wikibase Occurrence # 371833
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Date: | Tuesday 24 November 1987 |
Time: | 14:20 LT |
Type: | Cessna 152 |
Owner/operator: | Gunnel Aviation |
Registration: | N5418P |
MSN: | 15284941 |
Total airframe hrs: | 3457 hours |
Engine model: | LYCOMING O-235-N2C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Clemente, CA -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | Santa Monica, CA |
Destination airport: | Carlsbad, CA (KCRQ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A PARTIAL LOSS OF ENG POWER OCCURRED WHILE THE STUDENT PLT WAS ON A SOLO X-COUNTRY FLT. HE APPLIED CARB HEAT, BUT TO NO AVAIL. THE ENG CONTINUED TO RUN ROUGH & THE PLT MADE AN EMERGENCY LANDING ON UPWARD SLOPING TERRAIN. DURING THE LANDING ROLL, THE NOSE GEAR HIT A HOLE IN THE DIRT & THE ACFT NOSED OVER. AN EXAM OF THE ENG DISCLOSED THAT THE #3 EXHAUST VALVE RETAINING NUT HAD BACKED OFF UNTIL THE VALVE WOULD NOT OPERATE AS THE CRANKSHAFT WAS ROTATED. DURING MAINTENANCE ON THE PREVIOUS DAY, THE #3 VALVES HAD BEEN ADJUSTED.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX88LA054 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB LAX88LA054
Location
Revision history:
Date/time | Contributor | Updates |
26-Mar-2024 10:43 |
ASN Update Bot |
Added |
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