ASN Wikibase Occurrence # 372756
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 30 June 1987 |
Time: | 14:00 LT |
Type: | Cessna T210M |
Owner/operator: | Bartolomei, Harry |
Registration: | N761JM |
MSN: | 62294 |
Engine model: | CONTINENTAL TSIO-520R |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tracy, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Hayward, CA (KHWD) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRCRAFT COLLIDED WITH TERRAIN AFTER A TOTAL LOSS OF POWER. THE PLT INDICATED THAT THE ENG FAILED AT 3,500 FT MSL. THE PLT HAD FLOWN FOR ABOUT 30 MIN WITH THE FUEL SELECTOR IN THE RIGHT TANK POSITION WHEN THE ENG QUIT. HE INITIALLY SWITCHED THE FUEL SELECTOR FROM THE RIGHT TANK TO THE LEFT TANK AND WAS UNABLE TO RESTART THE ENG. HE ATTEMPTED TO RESTART THE ENG SEVERAL MORE TIMES ALTERNATING THE FUEL TANK SELECTOR POSITION. EXAM OF THE ACFT REVEALED THE RIGHT FUEL TANK WAS EMPTY ADN THE LEFT TANK CONTAINED FUEL. FURTHER EXAM OF THE ACFT DID NOT REVEAL ANY MALFUNCTIONS. THE PLT INDICATED THAT HE ESTIMATED THE FUEL QUANTITY BASED ON PREVIOUS ACFT USE AND EXAM OF THE FUEL QUANTITY GUAGES.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX87LA251 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB LAX87LA251
Location
Revision history:
Date/time | Contributor | Updates |
26-Mar-2024 21:10 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation