ASN Wikibase Occurrence # 373469
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Date: | Saturday 7 March 1987 |
Time: | 17:30 LT |
Type: | Beechcraft BE 36 |
Owner/operator: | Bonanza Aircraft Leasing Co. |
Registration: | N12KT |
MSN: | E-1193 |
Year of manufacture: | 1977 |
Total airframe hrs: | 1587 hours |
Engine model: | CONTINENTAL IO 520 8A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Alma, MI -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Grand Rapids, MI (GRR |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:ACCORDING TO THE PLT, DURING THE PREFLIGHT INSPECTION, HE DETERMINED THAT BOTH GAS TANKS WERE FULL AND 'EVERYTHING WAS IN ORDER.' AFTER APRX ONE HOUR OF LOCAL FLIGHT, THE PLT ENTERED A LEFT DOWNWIND FOR RWY 27 AT GRATIOT COMMUNITY AIRPORT, ALMA, MICHIGAN. THE PLT STATED THAT HE THEN SWITCHED TO THE OTHER FUEL TANK, WHICH WAS FULL, AND SHORTLY THEREAFTER 'ENCOUNTERED ENGINE OUT.' ACCORDING TO THE PLT, HE OBSERVED THE TANK INDICATOR AND CHECKED THE FUEL SLECTOR VALVE, WHICH 'SEEMED TO BE FIRMLY IN PLACE.' THE ACFT LANDED SHORT OF THE RWY, IN A DITCH PARALLEL TO THE RWY. INSPECTION OF THE ACFT REVEALED THAT THE ENGINE HAD NO FUEL IN ITS SYSTEMS. THE #6 FUEL LINE FROM THE FUEL SELECTOR VALVE TO THE ENGINE DRIVEN FUEL PUMP WAS DRY. WHEN THE SELECTOR VALVE WAS MOVED TO THE LH AND RH POSITIONS, WITH THE ELECTRIC FUEL BOOST PUMP ON, THE ENGINE HAD FUEL FLOW OUT OF THE ENGINE FUEL PUMP OUTLET TO THE FUEL CONTROL.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI87LA091 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB CHI87LA091
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 13:25 |
ASN Update Bot |
Added |
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