ASN Wikibase Occurrence # 373773
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 27 December 1986 |
Time: | 17:30 LT |
Type: | Cessna 150H |
Owner/operator: | Private |
Registration: | N7190S |
MSN: | 15867890 |
Total airframe hrs: | 3087 hours |
Engine model: | CONTINENTAL O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Harrison, OH -
United States of America
|
Phase: | Initial climb |
Nature: | Training |
Departure airport: | Harrison, OH (I67) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ENGINE QUIT AFTER TAKEOFF AT ABOUT 200 FT AGL. A LDG WAS MADE IN A PLOWED FIELD WHERE THE ACFT FLIPPED OVER INVERTED. THE CFI PIC REPORTED THAT, PRIOR TO TAKEOFF, HE HAD CALCULATED THERE WAS ADEQUATE FUEL ON BOARD FOR THE FLT; HIS CALCULATIONS WERE BASED ON AN ASSUMED PRIOR ACFT USAGE OF 3.9 HRS AND FUEL TANK GAGE READINGS NEAR 1/4 FULL. INFORMATION OBTAINED FROM THE ACFT OPERATOR INDICATED THAT THE ACFT WAS LAST REFUELED 5.1 HRS PRIOR TO THE ACCIDENT. POST-CRASH EXAMINATION OF THE ACFT REVEALED NO EVIDENCE OF FUEL IN THE ACFT SUMPS OR CARB FUEL BOWL. A POST-CRASH TEST RUN OF THE ENGINE REVEALED NO DISCREPANCIES.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL87DEG02 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB ATL87DEG02
Location
Revision history:
Date/time | Contributor | Updates |
27-Mar-2024 17:07 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation