ASN Wikibase Occurrence # 374519
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 28 July 1986 |
Time: | 10:00 LT |
Type: | Cessna 195 |
Owner/operator: | Private |
Registration: | N3899V |
MSN: | 7377 |
Year of manufacture: | 1949 |
Total airframe hrs: | 5931 hours |
Engine model: | JACOBS R755A2 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ramona, CA -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Gillespie, CA (KSEE) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRCRAFT OWNER STATED THAT THE PURPOSE OF THE FLIGHT WAS TO OBTAIN 5 HOURS OF TRANSITION TRAINING IN THE TAIL DRAGGER AND ACCOMPLISH A BFR. AFTER DEPARTURE THE CFI HAD THE PILOT PERFORM AIRWORK MANEUVERS ENROUTE TO THE RAMONA AREA. THE PILOT SAID THAT A LIGHT OIL FILM HAD DEVELOPED ON THE WINDSHIELD DURING THE AIRWORK AND A DECISION WAS MADE TO LAND AT ROMONA TO CLEAN THE WINDSHIELD AND PRACTICE TAKEOFFS AND LANDINGS. INTENDING TO MAKE A THREE POINT LANDING, THE PILOT SAID THAT A 'SLIGHT BOUNCE OCCURRED ON TOUCHDOWN' AND THE CFI TOLD HIM TO ADD A LITTLE POWER. THE PILOT SAID THAT HE COMPLIED AND THEN THE CFI TOLD HIM 'NO,' AND 'YANKED THE THROTTLE OFF.' THE PILOT SAID THAT AFTER THE CFI REDUCED THE POWER THE AIRCRAFT 'WENT WILD AND TURNED SIDEWAYS.' THE PILOT FURTHER SAID THAT THE CFI 'GRABBED THE CONTROLS' AS HE REDUCED THE THROTTLE TO IDLE. ACCORDING TO THE PILOT'S REPORT, THE CFI HAD ONLY 11 HOURS TOTAL IN THE CESSNA 195, WITH ONLY ONE HOUR ACCRUED IN THE PAST 90 DAYS.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX86LA306 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB LAX86LA306
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
28-Mar-2024 10:15 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation