ASN Wikibase Occurrence # 374543
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Date: | Friday 25 July 1986 |
Time: | 17:05 LT |
Type: | Huizenga SEA HAWK |
Owner/operator: | Craig D.huizenga |
Registration: | N85CK |
MSN: | 015 |
Total airframe hrs: | 1 hours |
Engine model: | LYCOMING O-320 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Clinton, IA -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Clinton, IA (KCWI) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING A TEST FLT OF AN EXPERIMENTAL SEA PLANE, THE PLT RPTD A LOSS OF ENG PWR DURING A TURN IN THE TRAFFIC PATTERN AT CLINTON AIRPORT. THE PLT STATED HE HAD 5 GALLONS OF FUEL ONBOARD AND HAD FLOWN ABOUT 2 TENTHS OF AN HOUR. INSPECTION OF THE FUEL SYSTEM REVEALED THAT DURING TURNS WITH LOW FUEL QUANTITY THE FUEL TANK WOULD BECOME UNPORTED AND THE ENG WOULD QUIT. NO FUEL TANK BAFFLES WERE INSTALLED IN THE TANK TO PREVENT THE FUEL FROM MOVING OUTBOARD FROM THE FUEL LINES. THE PLT STATED THAT THIS PROBLEM WOULD BE CORRECTED WITH THE INSTALLATION OF BAFFLES IN THE TANKS.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MKC86LA160 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB MKC86LA160
Location
Revision history:
Date/time | Contributor | Updates |
28-Mar-2024 10:28 |
ASN Update Bot |
Added |
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