ASN Wikibase Occurrence # 375018
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 25 May 1986 |
Time: | 20:05 LT |
Type: | Mooney M20 |
Owner/operator: | Private |
Registration: | N6519B |
MSN: | 1186 |
Year of manufacture: | 1966 |
Total airframe hrs: | 4112 hours |
Engine model: | LYCOMING O-320-A |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fargo, ND -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Grand Forks, ND (GFK |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT REPORTS THAT HE EXPERIENCED DIFFICULTY IN RETRACTING THE LANDING GEAR AFTER DEPARTURE BUT IT DID RETRACT AFTER SEVERAL ATTEMPTS. HE SAID THE GEAR SYSTEM SEEMED TO BE HANGING UP. UPON REACHING DESTINATION THE GEAR AGAIN SEEMED TO HANG UP WHEN EXTENSION WAS ATTEMPTED. AFTER SEVERAL ATTEMPTS TO LOWER THE GEAR THE GEAR HANDLE BROKE OFF AND ALL FURTHER ATTEMPTS TO EXTEND THE GEAR WERE FUTILE.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN86LA145 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB DEN86LA145
Revision history:
Date/time | Contributor | Updates |
28-Mar-2024 15:19 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation