ASN Wikibase Occurrence # 375335
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Date: | Friday 4 April 1986 |
Time: | 19:35 LT |
Type: | Piper PA-31-350 |
Owner/operator: | Key Largo Air Service |
Registration: | N55WE |
MSN: | 31-7405163 |
Total airframe hrs: | 6449 hours |
Engine model: | LYCOMING TIO-540-J2BD |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Homestead, FL -
United States of America
|
Phase: | En route |
Nature: | Ferry/positioning |
Departure airport: | Key West, FL (KEYW) |
Destination airport: | Homestead, FL (X51) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE FLT WAS NEARING COMPLETION OF A 4.2 HR X-COUNTRY FLT & WAS APRX 7 MILES FROM THE DEST WHEN BOTH ENGS QUIT DUE TO FUEL EXHAUSTION. A FORCED LDG WAS PERFORMED. THE PLT STATED THE ACFT HAD DEPARTED WITH A FULL FUEL LOAD OF 182 GALS. THE ACFT OWNER STATED THAT FUEL CONSUMPTION AVERAGED ABOUT 44 GALS PER HR. AT THAT RATE, THE ACFT WOULD HAVE CONSUMED APPROX 185 GALS. AFTER THE ACCIDENT, THE PLT STATED THAT A FACTOR IN THE ACCIDENT MAY HAVE BEEN THAT HE HAD BEEN RECENTLY FLYING ANOTHER PA-31 WHICH HAD A GREATER FUEL CAPACITY DUE TO THE INSTALLATION OF AUX FUEL TANKS & HE MAY HAVE SUBCONSCIOUSLY THOUGHT THAT HE HAD MORE FUEL THAN HE ACTUALLY HAD.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA86FA112 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB MIA86FA112
Location
Revision history:
Date/time | Contributor | Updates |
28-Mar-2024 18:50 |
ASN Update Bot |
Added |
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