ASN Wikibase Occurrence # 375388
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 27 March 1986 |
Time: | 00:41 LT |
Type: | Boeing 727-231 |
Owner/operator: | Trans World Airlines (TWA) |
Registration: | N52311 |
MSN: | 19830/633 |
Year of manufacture: | 1968 |
Total airframe hrs: | 44246 hours |
Engine model: | P&W JT8D-9A |
Fatalities: | Fatalities: 0 / Occupants: 96 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Boston, MA -
United States of America
|
Phase: | Taxi |
Nature: | Passenger - Scheduled |
Departure airport: | Saint Louis-Lambert International Airport, MO (STL/KSTL) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:TWO OF 3 REQD FLT ATTENDANTS (F/A'S) WERE DISTRIBUTING PASSENGER (PAX) COATS AS THE ACFT WAS BEING TAXIED AFTER LNDG. SMOKE FM AN OVERHEATED AIR COND (A/C) PACK BGN ENTERING THE CABIN & THE F/A'S RETURNED TO THEIR DUTY STATIONS. THE FLT CREW STOPPED THE ACFT AT THE GATE & SHUT DWN THE ENGS, BUT LEFT THE APU RUNNING TO PROVIDE ELECTRICITY FOR LIGHTING. THEF/A'S OPENED THE L FWD DOOR & GND PSNL OPENED THE REAR STAIR DOOR TO DEPLANE THE PAX. THE CAPT MADE AN ANNOUNCEMENT TO KEEP THE PAX CALM, BUT SMOKE BCM DENSE & PAX OPENED THE EMERG EXITS OVR THE WINGS & BGN EXITING FM THEM. TWO PAX RCVD MINOR INJURIES WHILE EXITING OVR THE WINGS. AN INVESTIGATION REVEALED THE ACFT HAD BEEN DISPATCHED WITH THE R PACK COOL-ING FAN INOP AS AUTHORIZED BY THE MIN EQUIP LIST (MEL). DRG FLT, A RADIO INTERFERENCE FILTER IN THE A/C SYS FAILED WHICHALLOWED THE FWD PACK SHUT-OFF VALVE TO OPEN, BUT NOT CLOSE. THIS PERMITTED APU AIR TO RUN THE AFFECTED PACK EVEN THO THESWITCH WAS OFF & A CIRCUIT BRKR WAS PULLED. WITH THE ENGS SHUT DOWN & THE R COOLING FAN INOP, THE SYS OVERHEATED.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC86IA093 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB NYC86IA093
Revision history:
Date/time | Contributor | Updates |
28-Mar-2024 19:24 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation