ASN Wikibase Occurrence # 375406
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Date: | Monday 24 March 1986 |
Time: | 13:10 LT |
Type: | Piper PA-23-250 |
Owner/operator: | Private |
Registration: | N77TS |
MSN: | 27-2665 |
Year of manufacture: | 1964 |
Total airframe hrs: | 5935 hours |
Engine model: | LYCOMING IO-540-C4B5 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Osteen, FL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Sanford, FL (KSFB) |
Destination airport: | Indiantown, FL (X58) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:BEFORE THE FLT, THE PLT & PAX WERE OBSERVED DRINKING ALCOHOLIC BEVERAGES ON THE WAY TO THE ARPT. AFTER MUCH DIFFICULTY TAXIING TO THE RWY, THE FLT WAS CLEARED FOR TAKEOFF AFTER ENTERING THE ACTIVE RWY WITHOUT CLEARANCE. AFTER TAKING OFF, THE ACFT WAS SEEN DEPARTING WITH THE GEAR STILL EXTENDED. SHORTLY AFTER DEPARTING, WITNESSES SAW THE ACFT NEAR A LAKE FLYING ERRATIC WITH THE RGT ENG SPUTTERING. SUBSEQUENTLY, THE ACFT DIPPED DOWN TOWARD THE WATER & MADE A RGT TURN. AT ABOUT THAT TIME, THE RGT WING CONTACTED THE WATER & THE ACFT CARTWHEELED & CRASHED. AN EXAM OF THE RGT ENG REVEALED THATTHE FUEL INJECTOR LINE TO THE #6 CYLINDER HAD FAILED UNDER A RUBBER GROMMET DUE TO FATIGUE. ALSO, THE FUEL SELECTORS WERE FOUND POSITIONED SO THAT BOTH ENGS WOULD FEED FROM THE LEFT OUTBOARD TANK, A CONDITION THAT WAS NOT RECOMMENDED FOR TAKEOFF. ADDITIONALLY, THE RGT PROP HAD NOT BEEN FEATHERED. TOXICOLOGY TESTS SHOWED THE PLT HAD A BLOOD/ALCOHOL LVL OF 289 MG/DL (0.289%) & THE PAX HAD 146 MG/DL (0.146%).
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA86FA103 |
Status: | Investigation completed |
Duration: | 2 years |
Download report: | Final report |
|
Sources:
NTSB MIA86FA103
Location
Revision history:
Date/time | Contributor | Updates |
28-Mar-2024 19:36 |
ASN Update Bot |
Added |
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