ASN Wikibase Occurrence # 376155
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 29 September 1985 |
Time: | 17:50 LT |
Type: | Mooney M20K |
Owner/operator: | Private |
Registration: | N231GW |
MSN: | 250250 |
Engine model: | CONTINENTAL TS10-360 SER |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Huntington Bch, CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Fullerton, CA (KFUL) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT ACKNOWLEDGED THAT ON SHORT FINAL APPROACH TO THE 2330 FT-LONG RWY, THE ACFT'S SPEED WAS 'A LITTLE HOT', & DURING LDG FLARE THE ACFT 'FLOATED IN GROUND EFFECT'. AFTER THE ACFT BOUNCED 3 TIMES THE PLT DECIDED TO GO AROUND & HE APPLIED FULL PWR. THE PLT FORGOT TO RAISE THE FLAPS FROM THEIR FULLY EXTENDED POSITION. THE ACFT OVERRAN THE RUNWAY'S END COLLIDING WITH A RWY LIGHT, 2 PARKED ACFT & A TRUCK, & IT CAME TO REST UPON IMPACTING A COMMERCIAL BLDG. WHICH HOUSED A FBO.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX85LA404 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB LAX85LA404
Revision history:
Date/time | Contributor | Updates |
29-Mar-2024 13:21 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation